N6530W

Substantial
None

Piper PA28S/N: 28-20609

Accident Details

Date
Thursday, July 2, 2020
NTSB Number
CEN20LA258
Location
Bridgeport, TX
Event ID
20200702X00420
Coordinates
33.162776, -97.824165
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

Maintenance personnel’s inadequate inspection, which resulted in a total loss of engine power due to a restricted air intake-induction system.

Aircraft Information

Registration
N6530W
Make
PIPER
Serial Number
28-20609
Engine Type
Reciprocating
Year Built
1964
Model / ICAO
PA28P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
REGISTRATION PENDING
Address
293 RIDGELINE DR
Status
Deregistered
City
CHICO
State / Zip Code
TX 76431-2052
Country
United States

Analysis

On July 1, 2020, about 1932 central daylight time, a Piper PA-28-140 airplane, N6530W, was involved in an accident near Bridgeport, Texas. The pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported the before takeoff engine run-up was normal. After takeoff, about 150 ft. above ground level, the engine seemed to lose power without any associated vibration, abnormal noise, or indications. The pilot’s attempts to determine the cause of the problem and restore engine power were not successful. He executed a forced landing “to a field of medium-maturity mesquite trees.”

A post-recovery engine examination revealed evidence consistent with an insect (mud dauber) nest within the carburetor heat induction system. Specifically, the inside surface of the carburetor heat shroud exhibited residue consistent with dirt/mud accretion. The engine exhaust tube common to the carburetor heat shroud exhibited a discoloration consistent with debris accretion. The discolored area on the exhaust tube coincided with the residue observed on the inside of the carburetor heat shroud. A fragment of compacted dirt was recovered from inside the carburetor heat duct, and the outboard end of the muffler exhibited a similar dirt/mud residue. No other anomalies were observed with respect to the engine installation.

According to the airplane maintenance records, an annual inspection was completed on September 14, 2017, at a recording tachometer of 2,701.58 hours. The next annual inspection based on the maintenance records was completed on June 29, 2020. The tachometer time corresponding to that inspection was 2,701.68 hours. The pilot reported that he purchased the airplane the same day as the most recent annual inspection. The accident occurred 2 days later, on July 1. The tachometer indicated 2,702.84 hours at the time of the postaccident examination.

The oil filter installed on the engine at the time of the postaccident examination was dated September 15, 2017. The tachometer time noted on the filter was 2,701.58 hours. The most recent inspection logbook entry did not include any reference to changing the engine oil and filter. However, the logbook entry corresponding to the prior inspection in 2017, which was conducted by the same mechanic, specifically noted that the engine oil and filter were replaced, and the old filter was opened and inspected for debris.

According to a graph in FAA Special Airworthiness Information Bulletin CE-09-35, Carburetor Icing Prevention, the weather conditions at the time of the accident corresponded to a slight possibility of carburetor icing at glide or cruise power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20LA258