N3412C

Substantial
None

Beech A23-24S/N: MA-357

Accident Details

Date
Sunday, July 19, 2020
NTSB Number
CEN20LA292
Location
Burns Flat, OK
Event ID
20200719X22746
Coordinates
35.381668, -99.201110
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

The mechanic’s improper maintenance when he reinstalled the fuel servo during the last annual inspection, which resulted in a loss of engine power during cruise flight when the throttle control rod-end disconnected from the fuel servo throttle linkage.

Aircraft Information

Registration
Make
BEECH
Serial Number
MA-357
Engine Type
Reciprocating
Year Built
1969
Model / ICAO
A23-24BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
A23-24

Registered Owner (Current)

Name
WILSON STEVE D
Address
20348 E 1230 RD
City
SENTINEL
State / Zip Code
OK 73664-5030
Country
United States

Analysis

On July 18, 2020, about 2245 central daylight time, a Beech A23-24 airplane, N3412V, was substantially damaged when it was involved in an accident near Burns Flat, Oklahoma. The pilot and his 3 passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that while established in cruise flight the airplane had a gradual loss of engine power. He was unable to restore engine power by switching fuel tanks, turning on the fuel boost pump, and advancing the throttle, mixture, and propeller controls full forward. The pilot made a forced landing in a grass field. After touchdown the airplane traversed over 3 large terraces, and the main landing gear collapsed when the pilot tried to swerve the airplane to avoid a tree. The horizontal stabilizer and both wings were substantially damaged during the forced landing.

The airplane was examined at the accident site by a Federal Aviation Administration airworthiness inspector. Both wing fuel tanks contained about 25 gallons of 100 low-lead aviation fuel. The throttle control was very loose when moved by hand in the cockpit. A visual examination revealed that the throttle control rod-end was not connected to the fuel servo throttle linkage. (Figure 1) The required retaining bolt, washer, and self-locking nut were not located during the investigation.

Figure 1. Throttle control rod-end found disconnected from the fuel servo throttle linkage.

The airplane had accumulated 8.72 flight hours since the last annual inspection that was completed on October 22, 2019. The inspection authorized (IA) mechanic who had completed the annual inspection stated that the fuel servo had been removed from the engine and overhauled in conjunction with the annual inspection. The IA mechanic stated that he personally reinstalled the overhauled fuel servo on the engine, while another individual moved the throttle and mixture controls in the cockpit. The IA mechanic stated that it is his standard practice to connect both the throttle and mixture controls to the fuel servo at the same time. The IA mechanic stated that he likely reused the bolt and washer to connect the throttle control rod-end to the fuel servo throttle linkage, and that it is also possible that he reused the self-locking nut. However, he would not have reused the self-locking nut if it had fully engaged the bolt threads by hand. The IA mechanic stated that he used two wrenches to secure the self-locking nut and that he did not use a torque wrench. A review of the Beech A23-24 Maintenance Manual revealed no specific assembly instructions on how to physically connect the throttle control rod-end to the fuel servo throttle linkage. The Beech A23-24 Illustrated Parts Catalog specified that the throttle control rod-end be attached to the fuel servo throttle linkage with a 169-910021 bolt, AN960-10 washer, and MS20365-1032 self-locking nut.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20LA292