N8244Y

Substantial
None

Piper PA 30S/N: 30-917

Accident Details

Date
Friday, June 5, 2020
NTSB Number
WPR20LA252
Location
Salem, OR
Event ID
20200728X51228
Coordinates
44.909442, -123.002500
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A fatigue failure of the right main landing gear trunnion.

Aircraft Information

Registration
Make
PIPER
Serial Number
30-917
Engine Type
Reciprocating
Year Built
1965
Model / ICAO
PA 30M600
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
6
FAA Model
PA-30

Registered Owner (Current)

Name
DOW JEFF
Address
PO BOX 1578
City
PORT HADLOCK
State / Zip Code
WA 98339-1578
Country
United States

Analysis

On June 4, 2020, at 1821 Pacific daylight time, a Piper PA30 airplane, N8244Y, was substantially damaged when it was involved in an accident at Salem, Oregon. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The pilot reported that after departure, he raised the landing gear and heard an unusual "clunk," but the landing gear retraction light illuminated normally and the mirror on the left engine nacelle indicated that the nose gear was retracted. The pilot continued the flight, and as the airplane neared the destination airport, he lowered the landing gear. The green “down and locked” light did not illuminate, and the nose landing gear door was open, but the nose landing gear was not extended. The pilot climbed the airplane and began to troubleshoot the issue, including performing the emergency gear extension procedure; however, “the system was totally jammed.” The pilot diverted to a nearby airport, where he performed a flyby, and ground personnel indicated that the main landing gear was partially extended, and the nose landing gear was not extended. The pilot landed the airplane and he and the passenger egressed without injury. The airplane sustained substantial damage to the keel beam and the right-wing spar.

Postaccident examination revealed that the right main landing gear trunnion was fractured. The trunnion was removed from the airplane and sent to the NTSB Materials Laboratory for analysis. The fracture surfaces had been forced together and taped before receipt by the laboratory, which inhibited examination. Most of the undamaged portions of the fracture surfaces exhibited a rough, fibrous texture with a dull luster. The inner mating fracture surface was less damaged and was sectioned below the fracture surface to facilitate further examination.

The sectioned portion was examined with a scanning electron microscope. Most of the surface exhibited features consistent with overstress fracture; however, there were two opposite facing areas exhibiting flatter, darker features. These areas were located at a tapered area where the trunnion and gusset were joined and showed evidence of fatigue striations that were consistent with having propagated from the outside surface inward. Due to post-fracture damage, only one crack initiation site was able to be observed, and this site exhibited an inward concave geometry inconsistent with a corrosion pit or pore.

The cross-sectional thickness of the tapered area in which the evidence of fatigue was found was measured as 0.4 inches. In contrast, the welded gusset was 0.8 inches thick, and the boss exhibited a diameter of 1.75 inches. This configuration would introduce a stress concentration at the locations of the fatigue cracking. The presence of two opposite-facing fatigue cracks was consistent with reverse bending fatigue, suggestive of the gusset bending back and forth at the interface. Once these fatigue cracks had propagated far enough into the boss cross section, the remainder of the part fractured under overstress during the last landing.

The chemical composition of the sectioned trunnion was examined using x-ray fluorescence (XRF) and energy dispersive x-ray spectroscopy (EDS). From the data obtained using these techniques, the trunnion was found to be consistent with an AA 2014 aluminum alloy. The hardness and conductivity met specifications consistent with peak hardened temper for this alloy.

The welded gusset however, exhibited a different chemical composition. The composition was consistent with an aluminum casting or welding alloy. The electrical conductivity was higher, and the hardness was softer than the Rockwell B scale and was, therefore, not measured conclusively. The hardness of the boss material was found to decrease as it was probed closer to the weld. These data were consistent with the boss being locally softened due to the heat inputs from the welding process.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20LA252