Accident Details
Probable Cause and Findings
The student pilot’s improper recovery from a power-off stall. Contributing to the accident was the flight instructor’s failure to properly monitor the student pilot during the stall recovery.
Aircraft Information
Registered Owner (Historical)
Analysis
On August 17, 2020, about 0756 central daylight time, a Czech Sport Sportcruiser airplane, N467SC, was substantially damaged when it was involved in an accident near Gober, Texas. The flight instructor and student pilot were seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.
According to the student pilot, he was performing a stall recovery maneuver after inducing a power-off stall. The student recalled that, when he felt the nose of the airplane begin to drop, he pitched the airplane nose down and applied full power. The student stated that, as the airspeed increased, he was unable to pitch the nose up or arrest the descent.
The flight instructor stated that, in guiding the student in performing a power off-stall, she directed him to pitch the airplane 10° nose high and hold right rudder to keep the airplane coordinated until it stalled. When the stall occurred, she instructed the student to pitch the airplane nose down 10o, increase power, and partially raise the flaps. The instructor recalled that the student pitched the airplane in a near-vertical attitude and added full power. The student turned the airplane’s yoke, and the airplane began to spin. The instructor took control of the airplane and attempted to recover the airplane from the spin but was unable to regain directional control.
Data from the airplane’s onboard avionics revealed that, at 1256:27, the airplane was configured with 30° flaps was 15° nose high with its airspeed slowing through the expected stall speed of 37 knots. The airplane’s pitch decreased, and, at 1256:32, the airplane was 60° nose low. At that time, the airplane began a roll to the right. At 1256:34, the airplane was 80° nose low and had rolled through 90° of right bank. The airplane continued to roll right until the airplane was inverted with a pitch attitude of about 50° nose low.
The flight instructor deployed the airframe parachute, and the airplane landed in an open field. Impact signatures showed that, after landing, the airplane was dragged across the field due to surface wind that had caught the parachute. The airplane flipped, and the empennage and wings sustained substantial damage. Neither pilot reported any flight control malfunction.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20LA339