Accident Details
Probable Cause and Findings
The pilot’s inability to maintain control of the helicopter due to a hydraulic system failure for reasons that could not be fully determined due to the thermal destruction from the postimpact fire.
Aircraft Information
Registered Owner (Historical)
Analysis
On August 19, 2020 about 0945 Pacific daylight time, an Arrow-Falcon Exporters, Inc., UH-1H, N711GH, was destroyed when it was involved in an accident near Coalinga, California. The pilot, the sole occupant was fatally injured. The helicopter was operated as a public use firefighting flight.
The accident flight was the pilot’s first day working the Hills Fire, which had started 4 days prior. The pilot took off at 0846 followed by another pilot who was flying a Bell 212 helicopter for another operator.
After departure, both helicopters flew south until reaching a small lake/reservoir (the dip site) to fill up the external load buckets attached to their respective helicopters. Thereafter, they flew to a predetermined area and began to unload their water on the fire. After releasing the water, they would return back to the dip site. After the accident pilot delivered about two buckets of water to one location he moved to another location delivering about five buckets of water.
The Bell 212 pilot recalled that after he departed the dip site with a bucket of water, he heard the accident pilot communicate over the air-to-air radio that he felt "abnormal noises and vibrations" and that he was going to make a precautionary landing. The Bell 212 pilot dumped his water and caught up to the accident helicopter with the intention of assisting the pilot in finding a good area to land. He remained a few hundred feet behind and above the accident helicopter. The accident helicopter was about 1,000 ft above ground level and maneuvering at an airspeed between 60 to 70 kts. The accident pilot then stated that the helicopter's "temps and pressures are good." A few seconds later the accident pilot stated "it's my hydraulics." The Bell 212 pilot relayed that he should make a right turn and fly down the ravine to less mountainous terrain (the flats).
Figure 1: Radar Data
The helicopter started to make a right turn and then banked back to the left while losing airspeed. The Bell 212 pilot noticed the helicopter still had its 100 ft longline and external load bucket attached and told the accident pilot to "release your long line and get forward airspeed," The accident pilot then stated "Mayday, Mayday, Mayday." The left turn steepened remaining in a level pitch attitude, and the helicopter began to make three or four 360° rotations (rapidly swapping the front and back), while drifting north-east. The helicopter then pitched in a nose-low, near vertical attitude and collided into terrain (see figure 2 below). A fire immediately erupted and the Bell 212 pilot made multiple trips to the dip site to fill his bucket and drop water on the accident site.
Figure 2: Pilot’s Statements Prior to Accident
WRECKAGE AND IMPACT
The helicopter came to rest on a 35° slope with the main wreckage about 25 yards downslope from the initial impact. Most of the wreckage was consumed by fire; the tail rotor assembly was intact. The tail rotor blades were intact, with no evidence of rotational scoring. The wreckage was recovered to a secure location for further investigation.
Airframe/Controls
The wreckage was highly fragmented and mostly consumed by a post-crash fire. The airframe sections that remained were parts of the tailboom, tail rotor, engine deck, cabin doors, landing skid tubes, one cross tube, and the engine. The main rotor head, blades, stabilizer bar, and upper transmission including the rotor mast were lost during the wreckage recovery.
The cockpit was highly fragmented and damaged by fire, with most of the instruments destroyed and unreadable. The engine control panel were separated from the center console and all the switches on the panel were deformed downward. The caution warning panel, located within the wreckage debris and separated from the instrument panel, sustained fire damage and the front plate was illegible due to sooting/melting. The interior of the panel exhibited similar damage and the individual annunciator capsule positions had shifted as a result so the original location of individual bulbs could not be determined. Nine intact bulbs with filaments were removed from the remnants of the panel, of which two exhibited hot filament stretching; their associated position could not be determined. The fuel valve switch had evidence of damage associated with impact and was unreliable for determining the switch position before impact.
Portions of the cockpit flight controls were identified, but a majority of the system was consumed by fire. The main flight control servos were separated from their input and output control rods. Fragments of both sections of the cyclic lateral control tubes and the lower mixing assembly were identified. The upper flight controls, consisting of the stationary and rotating swash plates and drive links, were not present for examination because they were dropped during recovery. The tail rotor control bell crank quadrant was not located. The tail rotor hydraulic servo was detached from the structure and sustained thermal damage; the input and output fittings were fractured. The tail rotor control forward cables, speed-rig turnbuckles, and aft cables remained within the tailboom.
The elevator spar remained in the tail section, and the left spar extended out of the left side of the tail boom. The elevator control horn assembly was in place in the tail section, and three elevator control bell cranks were identified.
Continuity of the hydraulic system could not be confirmed due to fire damage sustained following impact. The hydraulic pump was separated from the transmission and was missing the splined drive shaft. The hydraulic filter was separated from its mount, and the input/output connectors were fractured. The filter screen was removed, inspected, and no debris was identified. The main rotor head, both main rotor blades, upper transmission, and rotor mast were not recovered, but both stabilizer bar dampers were recovered. Photos from on scene showed chordwise marks on various portions of the unburned blade. The burned blade was too damaged to identify surface score marks from the photos taken.
Segments of the tail rotor drive shaft were numbered from 1 to 6, starting at the tail rotor drive output of the lower transmission. Drive shaft segments 1 to 3 were not recovered and were presumed to have been consumed by the post-crash fire. The drive-shaft bearing-end that connects to the transmission tail rotor drive quill was identified, as well as the drive shaft ends that mate with the support bearings for segments 1 to 3. The aft end of segment 4 was connected to segment 5 through the support bearing. Drive segment 5 was connected to the 42° gearbox, and drive segment 6 was connected from the 42° gearbox to the tail rotor 90° gearbox. One tail rotor blade showed no observable damage, while the other blade had chordwise dirt streaks and heat damage on the outboard half of its trailing edge. On the reverse side of that blade, the outboard 2/3 of the blade had fire damage to the skin and underlying layers. The blade also had a crease in the chordwise direction about 8 inches from the root.
The photos of the cargo hook on-scene and the post examination revealed that the hook portion had separated from its attachment hardware. The final location of the external load bucket is unknown, but the witness said he did not see the bucket being released.
Servos
The National Transportation Safety Board (NTSB) Materials Laboratory examined the left lateral hydraulic servo; right lateral hydraulic servo and its irreversible valve assembly; and the collective hydraulic servo for the main rotor of the helicopter.
The collective actuator, left lateral actuator, right lateral actuator, and an irreversible valve assembly were subjected to x-ray radiograph and computed tomography (CT) scanning to document each component’s internal condition. The results of the scan identified high density (metal) particles deep within the irreversible valve assembly.
The right lateral servo showed indications of exposure to a fire, including an oxide layer on the outer surface, micro-cracks, resolidified metal, and deformation damage. The upper housing was disassembled, and the ring seals were found to be fractured. The lower housing contained two circumferential inserts that functioned as raceways, which showed no evidence of wear or damage. The piston portion of the rod contained a groove that incorporated a ring seal, which also fractured into multiple pieces. The hydraulic servo cylinder contained an internal spool and sleeve assembly, but an attempt to pull the push-pull rod out of the port failed. No evidence of corrosion, gouge, or wear damage was found in any of the examined parts.
Disassembly of an irreversible valve assembly for a right lateral servo, revealed the internal valves, including a sequence valve, check valves "A" and "B," a differential pressure relief valve, and an accumulator valve. During disassembly, evidence of bending deformation damage was observed on the cover for the sequence valve, and the inner surface of the cover showed evidence of an oxide layer and micro-cracks. The piston head and sleeve contained ring seals that were fractured and could not be removed with needle-nose pliers. The internal parts of the sequence valve, check valves "A" and "B," and the differential pressure relief valve were intact, except for the fractured ring seals. The seat portion for the check valve "A" showed evidence of wear damage, while the seat portion for check valve "B" showed no evidence of wear.
The left lateral and collective servos were disassembled in a manner that was similar to the right lateral servo. The observations made on those servos were similar to those found on the right lateral servo, with the exception that the left lateral servo’s piston was completely retracted (the other servos were in various positions, but not at such an extreme). It could not be definitively determined if this signa...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20LA280