N4744M

Substantial
None

ZENITH CH 750S/N: 75-8874

Accident Details

Date
Wednesday, September 16, 2020
NTSB Number
CEN20LA397
Location
Montgomery City, MO
Event ID
20200917X31028
Coordinates
38.979721, -91.610000
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s inadequate fuel management and flight planning, which led to a total loss of engine power due to fuel exhaustion and a forced landing into rough terrain.

Aircraft Information

Registration
Make
ZENITH
Serial Number
75-8874
Engine Type
Reciprocating
Year Built
2015
Model / ICAO
CH 750
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
STOL CH 750 ZENITH

Registered Owner (Current)

Name
ZENSTOL LLC
Address
1060 COUNTY ROAD 2400 N
City
CARMI
State / Zip Code
IL 62821-4009
Country
United States

Analysis

On September 16, 2020, about 1253 central daylight time, an amateur-built Zenith CH 750 airplane, N4744M, was substantially damaged when it was involved in an accident near Montgomery City, Missouri. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot planned the flight from Kyle-Oakley Field Airport (CEY) Murray, Kentucky to Mexico Memorial Airport, Mexico (MYJ), Missouri. The pilot was making the first long cross-country flight in the airplane and estimated 22-23 gallons of fuel were onboard, with an expected fuel consumption rate of about 6 gallons per hour. After departing CEY about 0958, the engine sputtered and lost total power while approaching MYJ about 1251. The pilot made a forced landing into a bean field and the airplane nosed over, which damaged both wings and tail.

Examination of the airplane at the accident site the next day revealed all fuel lines were intact and undamaged, with no smell of fuel noticed. While the airplane was inverted, the right fuel tank cap was removed, and no fuel was observed. During recovery of the airplane four days after the accident, minimal fuel was noticed in the fuel lines and none of the soybean crops near the airplane were blighted.

At the recovery location, about ¼ cup of fuel was drained from the fuel strainer, with no indication of water. Both fuel tanks were refilled and held about 12 gallons in each tank, which was consistent with the flight manual. The fuel was drained, with no contamination noticed. No preimpact anomalies were observed during examination of the engine.

Review of the pilot’s handwritten flight notes revealed he considered a fuel stop between CEY and MYJ. Following the flight, the pilot stated the onboard fuel quantity indicating system was unreliable and that a fuel stop may have been warranted. Additionally, a new carburetor was installed about four months prior to the accident and the fuel consumption rate had not been verified with the new carburetor installed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20LA397