N4376Q

Destroyed
Serious

CESSNA 172S/N: 17260276

Accident Details

Date
Sunday, January 31, 2021
NTSB Number
CEN21LA119
Location
Silt, CO
Event ID
20210201102580
Coordinates
39.519800, -107.666700
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
3
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

The pilot’s failure to avoid powerlines while flying at low altitude.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17260276
Engine Type
Reciprocating
Model / ICAO
172C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172L

Registered Owner (Current)

Name
FRANKE RUSSEL G
Address
110 ESTHER CT
City
SILT
State / Zip Code
CO 81652-9831
Country
United States

Analysis

On January 31, 2021, about 1420 mountain standard time, a Cessna 172, N4376Q, was destroyed when it was involved in an accident near Silt, Colorado. The pilot and two passengers sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

A passenger’s family member reported that the purpose of the flight was to take some friends’ children flying in the local area. The family member stated that, while expecting the airplane to return for landing, he received a call from the mother stating that they had crashed.

The main wreckage was located about 3 miles east of the departure airport in an area of rising terrain. The debris field began about 25 ft past a set of high-tension transmission wires and extended about 670 ft. The upper 2 ft of the vertical stabilizer and rudder were located about 75 ft from the beginning of the debris field. The initial ground scar was located about 475 ft past the transmission wires and was identified by a damaged tree and sheet metal consistent with the color of the airplane. The main wreckage came to rest inverted about 600 ft past the wires.

A post-accident airframe examination revealed that the lower portion of the vertical stabilizer and rudder remained attached to the fuselage and exhibited damage consistent with an impact with a wire. The vertical stabilizer leading edge was deformed aft in a U-shaped direction with metal polishing and black paint transfer. Flight control continuity was established to the ailerons, elevators, and rudder, and the flaps were found in the retracted position. Internal continuity was established throughout the engine and valve train. All cylinders were examined with a borescope with no anomalies noted. No mechanical anomalies or malfunctions were found that would have precluded normal operation.

A cell phone video recording taken by a passenger from inside the airplane showed the airplane flying at low altitude, followed by an upset event and the subsequent impact sequence. The video did not capture a continuous forward view out of the cockpit windows.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN21LA119