N841BP

Destroyed
None

AEROSPATIALE AS350 B2 ECUREUILS/N: 2036

Accident Details

Date
Wednesday, May 12, 2021
NTSB Number
CEN21LA216
Location
Yukon, OK
Event ID
20210513103077
Coordinates
35.491833, -97.821178
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot receiving instruction’s untimely and unidentified inadvertent activation of the hydraulic cut-off switch, which turned off the hydraulic system while the helicopter was at slow airspeed followed by a rapid power increase, which resulted in a loss of control. Contributing was the pilot’s failure to relinquish control of the helicopter to the flight instructor when directed.

Aircraft Information

Registration
N841BP
Make
AEROSPATIALE
Serial Number
2036
Year Built
1987
Model / ICAO
AS350 B2 ECUREUIL

Registered Owner (Historical)

Name
US DEPARTMENT OF HOMELAND SECURITY
Address
1300 PENNSYLVANIA AVE NW RM 6.4A
Status
Deregistered
City
WASHINGTON
State / Zip Code
DC 20229-0002
Country
United States

Analysis

On May 12, 2021, about 1530 central daylight time, an Aerospatiale (Airbus) AS350 B2 helicopter, N841BP, was destroyed when it was involved in an accident near Yukon, Oklahoma. The pilot receiving instruction and the flight instructor were not injured. The helicopter was operated as a 14 CFR Part 91 public aircraft instructional flight.

According to the flight crew, the pilot receiving instruction (pilot) was enrolled in the US Customs and Border Protection Initial Pilot Certification course for the AS350 B2. The flight departed the Will Rogers International Airport (KOKC) and proceeded to the Clarence Page Municipal Airport (KRCE) to conduct training maneuvers. After arrival at KRCE, the flight crew conducted several approaches to the airport including confined area and pinnacle approaches. They then conducted several simulated emergencies, each of which required the helicopter’s hydraulic system to be turned off and then turned back on at the conclusion of the procedure. The hydraulic system was turned off and on using the hydraulic cut-off switch, an unguarded push-button switch mounted on the end of the pilot’s collective stick.

After the simulated emergencies, the flight crew proceeded to conduct a series of “quick stops.” After the third quick stop, the pilot heard a radio call indicating an airplane was on final approach to land on the runway they were using, and the flight instructor indicated that they would clear the runway. The pilot added that he completed a final quick stop and immediately entered a climbing left turn.

The pilot stated that in the turn, he noticed the helicopter yawing left, and his pedal inputs were unable to correct the yaw. When the pilot adjusted his grip on the collective, he felt the hydraulic cut-off button with his thumb as he prepared to reduce collective. As he tightened his grip on the collective, “the hydraulics came offline aggravating the left yaw into a hard left spin.” The controls were stiff, and the flight instructor told him to turn the hydraulics back on. The pilot “intentionally pressed the [hydraulic cut-off] button but felt no effect.” He pressed the button a second time, but the hydraulic light on the caution warning panel remained illuminated, so he pressed the button a third time.

The flight instructor reported that on the last quick stop, the helicopter slowed normally but then started a left yaw about 25 ft above ground level. After the helicopter yawed about 30° left of centerline, he pushed forward on the cyclic to gain airspeed. The flight instructor stated that “as the aircraft was recovering, the control loads instantly became excessive,” and he noticed the hydraulic light on the caution warning panel was illuminated. He told the pilot to turn on the hydraulics; however, the hydraulic pressure was never restored. The flight instructor told the pilot that he was taking control of the helicopter. However, the pilot did not relinquish control. The flight instructor attempted to regain control of the helicopter but was unable to overcome the high control loads.

The helicopter continued to spin, impacted the ground in a nose-down attitude, rolled over, and came to rest on its right side. Both occupants were able to exit the helicopter before a postimpact fire consumed most of the helicopter.

Examination of the helicopter was limited by the postimpact fire; however, no preimpact abnormalities were identified with helicopter’s airframe and engine.

The US Customs and Border Protection Air and Marine Operations Division reported that the agency’s selection process for the Air Interdiction Agent Program failed to properly identify that the pilot was not qualified for the program.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN21LA216