N6596K

Substantial
Serious

GRUMMAN ACFT ENG COR-SCHWEIZER G-164CS/N: 6C

Accident Details

Date
Wednesday, May 12, 2021
NTSB Number
WPR21LA200
Location
Glenn, CA
Event ID
20210519103110
Coordinates
39.479139, -122.062130
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s fuel mismanagement, which resulted in fuel exhaustion, a total loss of engine power, and an off-airport hard landing.

Aircraft Information

Registration
Make
GRUMMAN ACFT ENG COR-SCHWEIZER
Serial Number
6C
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
G-164CG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
G-164C

Registered Owner (Current)

Name
JONES AVIATION INC
Address
PO BOX 497
City
BIGGS
State / Zip Code
CA 95917-0497
Country
United States

Analysis

On May 12, 2021, about 1030 Pacific daylight time, a Grumman ACFT ENG CORSchweizer G-164C, N6596K, was substantially damaged when it was involved in an accident near Glenn, California. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 137 agricultural flight.

The pilot reported that the airplane had just departed with the fuel gauge indicating a half-full tank of fuel and a full load of product (2,200 pounds of rice seed). About 100 ft above ground level the engine lost total power. He saw a narrow dirt frontage road in between rice fields and made a forced landing, during which the airplane landed hard and came to rest upright, causing substantial damage to the wings and fuselage. The pilot reported that he did not refuel the airplane before the accident flight based on the fuel gauge indications.

The operator reported that the center fuel tank, which draws fuel from the two wing tanks was empty of fuel. About 1 gallon of fuel was recovered from the fuel sump. The engine and the fuel systems remained intact and uncompromised. Maintenance personnel reported that they checked the fuel gauge in the cockpit, and it revealed that the center fuel tank was indicating half full. When the float connected to an arm in the center tank was manipulated, the fuel gauge in the cockpit moved but not in a manner coincident with the placement of the float, and that the fuel gauge may have been reporting false quantities of fuel.

The engine was sent to a repair facility for overhaul with no discrepancies identified. Further testing of the fuel gauge was not accomplished.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR21LA200