N2143G

Destroyed
Serious

PIPER PA-28-161S/N: 28-7916176

Accident Details

Date
Thursday, June 24, 2021
NTSB Number
ERA21LA267
Location
Easton, MD
Event ID
20210624103329
Coordinates
38.813886, -76.065659
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined.

Aircraft Information

Registration
N2143G
Make
PIPER
Serial Number
28-7916176
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
PA-28-161P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
TRIDENT AIRCRAFT INC
Address
9475 JET LANE
Status
Deregistered
City
EASTON
State / Zip Code
MD 21601
Country
United States

Analysis

On June 24, 2021, about 1115 eastern daylight time, a Piper PA-28-161, N2143G, was destroyed when it was involved in an accident near Easton, Maryland. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the student pilot, he conducted a preflight inspection before he and his instructor completed the engine run-up and takeoff with no anomalies noted. They stayed in the airport traffic pattern, conducting three takeoffs and landings before stopping to let the instructor out, so that the student pilot could perform three solo take-offs and landings.

After the second take-off, the student pilot was turning onto the downwind leg of the airport traffic pattern when he heard a reduction in engine power and could see the propeller slowing down. He was at an altitude of about 700 ft above ground level and had to pitch the airplane forward so it would not stall. The pilot did not think he could make it back to the airport, so he selected a field and maneuvered for a forced landing, during which the airplane impacted a pile of metal on the ground.

Witnesses reported that the airplane appeared to pitch nose-up before reaching the field, then stalled and impacted a construction area. Ground personnel rescued the student pilot before a postcrash fire ensued.

The wreckage was taken to an aircraft recovery facility for further examination. The fuselage above the lower fuselage skin and structure below the floorboards was consumed by fire. The instrument panel, most of the instruments, avionics, gauges, and switches were fire damaged and unreadable. The firewall was separated from the fuselage and the rudder pedal assembly remained attached to the firewall. Flight control cable continuity for the aileron, stabilator, and rudder cables were continuous from the cockpit to the respective control surfaces, except for separations consistent with cuts made during the recovery process near the wing roots and the tailcone.

The propeller remained attached to the crankshaft flange. Both magnetos remained installed on the back of the accessory housing; however, both units were consumed by fire. The cylinders were examined using a borescope and minor scoring was noted. No anomalies were noted with the engine or airframe that would have precluded normal operation. Due to fire damage, the ignition and fuel systems could not be tested.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA21LA267