N67CW

Substantial
None

BEECH A36S/N: E-1069

Accident Details

Date
Tuesday, August 24, 2021
NTSB Number
CEN21LA382
Location
Granbury, TX
Event ID
20210824103747
Coordinates
32.340946, -97.646717
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power for reasons that could not be determined with the available information.

Aircraft Information

Registration
N67CW
Make
BEECH
Serial Number
E-1069
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
A36BE36
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HUMANITY2OTHERS LLC
Address
4103 KING AIR CT
Status
Deregistered
City
GRANBURY
State / Zip Code
TX 76049-2336
Country
United States

Analysis

On August 24, 2021, about 1030 central daylight time, a Beech A36 airplane, N67CW, was substantially damaged when it was involved in an accident near Granbury, Texas. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported to the responding Federal Aviation Administration (FAA) inspector that shortly after departure from the Pecan Plantation Airport (0TX1), the engine lost power. The pilot selected a nearby field for a forced landing. An inspection of the airplane by the FAA inspector noted damage to the airplane’s wings and fuselage. Fuel was available in the airplane’s fuel tanks and the fuel selector was positioned to the left tank. The engine had about 8 quarts of oil in it. (See figure 1)

Figure 1: Accident airplane FAA photo

During recovery of the airplane, about 80 gallons of fuel, split evenly between the fuel tanks, were recovered from the airplane.

After the wreckage was recovered, an examination and test run were conducted. The fuselage, minus the wings, was strapped down to a trailer. The top engine cowling was removed, and a visual inspection of the engine did not reveal any pre-impact abnormalities. A fuel canister was connected to the airplane’s fuel line on the airplane’s left side. The engine started without hesitation or delay and was then warmed up at idle rpm. The throttle was advanced, and a magneto check was completed; no anomalies were noted. Full throttle was then applied, and the engine responded accordingly.

Before and after the test run, data from the engine monitor was downloaded. The data did not illustrate any abnormalities with either the cylinder head temperature or exhaust gas temperatures that were recorded; the total loss of power was evident. The airplane’s fuel tanks, and main fuel strainer were checked for contaminates/blockage. No abnormalities were noted during the examination and engine test run and the engine appeared to make rated power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN21LA382