Accident Details
Probable Cause and Findings
The total loss of engine power for reasons that could not be determined based on available information.
Aircraft Information
Registered Owner (Historical)
Analysis
On September 2, 2021, about 1045 central daylight time, a Beech A35 airplane, N8419A, was substantially damaged when it was involved in an accident near Morrilton, Arkansas. The pilot and passenger sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The passenger reported that he recently purchased the airplane and that he and the pilot were in the process of flying it to his home airport. The pilot and passenger flew the airplane before the purchase and for familiarization before the accident flight and the airplane operated normally.
For the accident flight, they departed the Ada Regional Airport (ADH), Ada, Oklahoma, about 0910 with an intended fuel stop at the Searcy Municipal Airport (SRC), Searcy, Arkansas, a distance of about 244 nautical miles. The pilot reported that the airplane’s cruise altitude was 8,500 ft. msl., and they had the left fuel tank for about 1.25 hours. He then switched to the rear auxiliary fuel tank and fuel pressures were normal.
About 7 to 8 minutes later, the engine suddenly lost all power, but the propeller remained windmilling. The pilot switched the fuel selector from the rear auxiliary tank to the right tank and attempted to restart the engine to no avail. He then switched to the left tank and after descending through a cloud layer was again unable to restart the engine. After descending below the clouds, the pilot switched to the right fuel tank again and power was restored for 5 to 10 seconds but then all engine power was again lost. The pilot attempted to glide the airplane to the Morrilton Municipal Airport, Morrilton, Arkansas, but had insufficient altitude. The airplane impacted trees and became suspended in the trees. The airplane sustained substantial damage to both wings and the fuselage.
Postaccident examination of the airplane and engine did not reveal any preimpact mechanical failures or malfunctions that would have precluded normal operation. An examination of the fuel system showed fuel in the lines and in the fuel selector. A bench test of the electric fuel pump shoed normal operation. Both fuel tanks had been breached during impact and determination of fuel quantity was not possible.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN21LA405