Accident Details
Probable Cause and Findings
The separation of the airplane’s elevator control push-pull tube, which resulted in a loss of control during the approach.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn October 14, 2021, about 1551 eastern daylight time, an experimental amateur-built Velocity SE RG airplane, N755V, was destroyed when it was involved in an accident near Space Coast Regional Airport (TIX), Titusville, Florida. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot owned the airplane, which was based at TIX. The airplane flew uneventfully from TIX to Sebastian Municipal Airport (X26), Sebastian, Florida, earlier during the day of the accident. While at X26, the pilot visited the airplane kit manufacturer’s facility to replace a landing-gear-up switch fuse because the landing gear was not retracting. Afterward, the pilot removed the pilot seat and the rear seat from the airplane and left the rear seat at the facility so that maintenance technicians could match color and specifications ahead of an interior aesthetics renovation planned for the next month. The pilot then reinstalled the pilot seat and departed X26 uneventfully about 1528 for the return flight to TIX.
According to witness statements, automatic dependent surveillance-broadcast data, and airport surveillance video, while the airplane was on short final approach to runway 9 at TIX, the airplane pitched up, climbed about 300 ft, then descended nose down. The airplane impacted a grass area about 400 ft right of the runway centerline and about 2,000 ft from the runway threshold. A postcrash fire ensued that consumed most of the wreckage. PERSONNEL INFORMATIONThe pilot’s logbook was not recovered. The president of the airplane kit manufacturer, who knew the pilot, estimated that the pilot had about 200 hours of total flight experience in the accident airplane make and model. AIRCRAFT INFORMATIONThe maintenance logbooks were not recovered. The pilot purchased the airplane in 2016, about 10 years after it was assembled. AIRPORT INFORMATIONThe maintenance logbooks were not recovered. The pilot purchased the airplane in 2016, about 10 years after it was assembled. WRECKAGE AND IMPACT INFORMATIONThe airplane came to rest upright and oriented along a magnetic heading of about 230°, and no debris path was observed. The cockpit and cabin were mostly consumed by fire. The flight control stick was not recovered. The pilot seat was identified, and the four bolts and their respective hard points remained attached. The pilot seat pin was also identified, but the seat frame was bent and separated, consistent with impact forces.
A Grand Rapids primary flight display and multifunction display were recovered and retained for data download. Both displays required an installed USB flash drive to record data, but no USB flash drives were installed in the units or recovered in the wreckage.
The left and right ailerons separated from their respective wings and were recovered near the wings. Aileron control continuity was confirmed from the separated ailerons to cables, a bellcrank, torque tubes, and the cockpit. The canard spar was intact but fire damaged and the left and right elevators were not recovered and presumed destroyed in the fire. The elevator push-pull tube section that connected to the control stick was recovered with no threaded rod end engaged, and the rod end was not recovered. Continuity of the elevator was confirmed from the torque tubes to the cockpit except for the push-pull tube section, which was retained for metallurgical examination. The elevator trim actuator was destroyed, and the preimpact elevator trim setting could not be determined. The left rudder was identified, and the right rudder was not recovered and presumed destroyed. The left rudder bellcrank remained intact, and its cable exhibited a broomstraw separation.
The engine separated from the airframe and came to rest upright. The three propeller blades remained attached to the hub, and all three blades separated about 12 inches from their respective roots. The top spark plugs were removed; their electrodes were intact and light gray in color. Borescope examination of the cylinders revealed no anomalies. The rear accessory section sustained thermal damage. After the rear accessory section was removed, the crankshaft could be rotated by hand. Camshaft, crankshaft, and valvetrain continuity were confirmed, and thumb compression was attained on all cylinders. Due to thermal damage, the ignition and fuel systems could not be tested.
Metallurgical examination of the elevator push-pull tube section revealed that it had been exposed to fire, causing a portion of the tube to collapse and melt. No contact marks from the jam nut were observed, and the first three threads in the threaded plug were missing. Examination with a stereo microscope revealed that the first three threads were fractured in shear overstress and that the remaining threads remained intact. ADDITIONAL INFORMATIONReview of the airplane kit assembly manual revealed instructions to have at least 0.5 inches of thread engagement with the rod end in the 1.5-inch threaded plug. A note indicated, “all the way in is best.” Due to a lack of maintenance documentation recovered, the investigation could not determine when the rod end had been most recently adjusted (for more information, see Materials Laboratory Factual Report in the public docket for this accident). MEDICAL AND PATHOLOGICAL INFORMATIONAn autopsy was performed on the pilot by the Office of the Medical Examiner for Brevard County, Rockledge, Florida. His cause of death was multiple blunt force injuries.
Toxicology testing performed on the pilot by the Federal Aviation Administration Forensic Sciences Laboratory identified doxylamine in the pilot’s cavity blood (80 ng/ml) and in his liver. Doxylamine is a sedating antihistamine available over the counter in various products intended to treat allergy and cold symptoms and induce sleep. It carries specific warnings about sleepiness. The usual blood level in which effects would be expected in live people is between 50 and 200 ng/ml.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA22FA015