N8038Z

Substantial
None

BEECH A36S/N: E-2568

Accident Details

Date
Thursday, December 2, 2021
NTSB Number
CEN22LA059
Location
Cleveland, TX
Event ID
20211206104356
Coordinates
30.401525, -95.053575
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

A total loss of engine power due to fuel starvation, the reason for which could not be determined.

Aircraft Information

Registration
Make
BEECH
Serial Number
E-2568
Engine Type
Reciprocating
Year Built
1990
Model / ICAO
A36BE36
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
A36

Registered Owner (Current)

Name
BAS PART SALES LLC
Address
575 ED BEEGLES LN
City
GREELEY
State / Zip Code
CO 80631
Country
United States

Analysis

On December 2, 2021, about 1415 central standard time, a Beech A36, N8038Z, was substantially damaged when it was involved in an accident near Cleveland, Texas. The pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that while en route at 6,000 ft on an instrument flight rules flight plan the airplane engine suddenly lost power. He reported that he was not in the process of changing or manipulating any controls at the time of the power loss. The pilot elected to fly toward a nearby airport depicted on his GPS receiver. While gliding toward the airport, he attempted to restart the engine several times, but he could not get fuel flow back even with the fuel pump on. He attempted switching fuel tanks during this time and the airplane engine monitor showed no fuel flow despite restart attempts.

During the descent, the airplane broke out of the clouds about 3,000 ft. The pilot realized that he would not be able to reach the airport he had selected and redirected the airplane toward a nearby highway.

During the landing flare on the highway, the right-wing tip struck a road sign. The airplane exited the highway and came to rest nose down in a ditch. The fuselage sustained substantial damage.

The pilot reported that he was utilizing the fuel flow indicator during the flight to aid in balancing fuel during the flight. He noted that he would switch tanks after about every 10 gallons burned.

When the airplane was recovered from the accident site, recovery personnel drained 22 gallons from the right-wing fuel tanks and 26 gallons from the left-wing fuel tanks.

A postaccident engine test run was conducted. The airplane’s wings had been removed and a temporary fuel can plumbed into the left wing fuel line for the test run. The propeller was bent and was replaced with a surrogate propeller for the test run. The engine started on the first attempt and ran without any problems or malfunctions.

The J.P. Instruments, Inc., EDM-900 engine monitor was removed from the airplane for subsequent download of stored data. The data supported the pilot’s description that the fuel flow dropped and the engine lost power with a corresponding loss of exhaust gas temperatures and cylinder head temperatures.

The reason for the interruption of fuel flow could not be determined during the postaccident airplane examination.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA059