N9500E

Substantial
None

AERONCA 11ACS/N: 11AC-1135

Accident Details

Date
Tuesday, February 8, 2022
NTSB Number
WPR22LA099
Location
Napa, CA
Event ID
20220216104651
Coordinates
38.462184, -122.214900
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power for undetermined reasons, which resulted in an off-airport landing on unimproved terrain.

Aircraft Information

Registration
Make
AERONCA
Serial Number
11AC-1135
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
11ACAB11
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
11AC

Registered Owner (Current)

Name
MCQUEEN TROY J
Address
837 CORTEZ WAY
City
LODI
State / Zip Code
CA 95242-3510
Country
United States

Analysis

On February 8, 2022, about 0845 pacific standard time, an Aeronca 11AC Chief, N9500E, was substantially damaged when it was involved in an accident near Napa, California. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he departed University Airport (EDU), Davis, California, and was enroute to Sonoma County Airport (STS), Santa Rosa, California. At approximately 30 minutes into the flight, about 20 nm north of Napa, California, the engine lost all power. The pilot stated that the engine “got quiet,” the “tach[ometer] dropped,” and the airplane could not maintain altitude. He immediately verified the throttle was full forward and then pulled the carburetor heat to the OPEN position. However, the airplane continued to descend. The pilot made mayday calls and performed a forced landing to a field, during which the airplane sustained substantial damage to the fuselage tubular frame.

A postaccident examination of the airframe did not reveal any preimpact mechanical anomalies. Examination of the engine cylinders and case did not reveal any indications of catastrophic engine failure. Mechanical continuity was established throughout the rotating group, valvetrain, and accessory section as the crankshaft was manually rotated at the propeller by hand. Thumb compression was achieved at all four cylinders and the valves displayed normal lift when the crankshaft was rotated. When the propeller was rotated by hand, spark was produced on all ignition leads, however, was “extremely weak.” Both magnetos were removed for further examination.

The mechanic who completed a postaccident examination of the right magneto stated that the magneto was unmaintained and in poor overall condition. The point cover screws were both stripped and cross threaded but still had the safety wire in place. The distributor axle set screw and bushing was worn and loose. The distributor gear had six gear teeth damaged and partially missing. The right magneto functioned within manufacturer standards during its bench test.

The left magneto was also unmaintained and in poor overall condition. The axle set screw was displaced and found at the bottom of the magneto housing. The distributor gear had over half of its teeth worn or missing. The distributor axle bushing was loose and worn, and the distributor axle bearing had failed. The left magneto functioned outside manufacturer standards during its bench test.

A review of the engine logbook revealed that the engine was last overhauled in 2007, about 400.7 hours prior to the accident. Subsequent log entries did not reveal that either magneto was overhauled or inspected more recently.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR22LA099