N823MM

Substantial
Minor

CZECH SPORT AIRCRAFT A S SPORTCRUISERS/N: C0526

Accident Details

Date
Friday, March 25, 2022
NTSB Number
WPR22LA137
Location
Lanark, NM
Event ID
20220329104854
Coordinates
31.984112, -106.809730
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s loss of control of the airplane after the inadvertent unlocking and opening of the canopy for reasons that could not be determined based on available evidence.

Aircraft Information

Registration
Make
CZECH SPORT AIRCRAFT A S
Serial Number
C0526
Engine Type
4-cycle
Year Built
2015
Model / ICAO
SPORTCRUISERAT2P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
SPORTCRUISER

Registered Owner (Current)

Name
CARPENTER ALAN L
Address
121 E REDD RD
City
EL PASO
State / Zip Code
TX 79932-1981
Country
United States

Analysis

On March 24, 2022, about 1845 mountain daylight time, a Czech Sport Aircraft Sportcruiser airplane, N823MM, was substantially damaged when it was involved in an accident near Lanark, New Mexico. The pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot stated the purpose of the flight was to calibrate a new angle-of-attack gauge that had been recently installed in the airplane. He climbed the airplane to an altitude of about 6,500 ft mean sea level and performed a power-off stall. As the nose of the airplane dropped, the left canopy latch “broke loose.” About 4 to 5 seconds later, the right canopy latch “blew open,” and the entire windscreen “popped up like a speed brake.” The airplane’s pitch remained nose down and the airplane impacted terrain, substantially damaging the left wing and fuselage. GPS data from a recovered device were consistent with the pilot’s statement.

Postaccident examination of the wreckage revealed no preimpact anomalies with the canopy or canopy operating system. The canopy locking handle was located on the back console panel between the two cockpit seats and was attached to a connecting rod equipped with identical locking hook mechanisms on each side of the fuselage/canopy opening. The canopy locking mechanisms disengaged and engaged simultaneously when the handle was manipulated. The locking mechanisms disengaged when the locking handle was pulled up and engaged fully (locked) when it was pushed fully down into a stowed position. The locking mechanisms consisted of a welded tab on the connecting rod joined to a pushrod that was attached to the canopy latch.

When the canopy locking handle was lifted, an over-center position was reached after about 1/4 inch of upward movement of the locking handle. The locking handle traveled about 3 additional inches before the locking mechanisms reached the fully disengaged position.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR22LA137