N321PF

Destroyed
Fatal

DIAMOND AIRCRAFT IND INC DA 40S/N: 40.375

Accident Details

Date
Sunday, April 24, 2022
NTSB Number
WPR22FA164
Location
Cedar City, UT
Event ID
20220424104989
Coordinates
37.647850, -112.973820
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
4
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot’s failure to maintain obstacle clearance, which resulted in controlled flight into terrain. Contributing to the accident was the pilot’s decision to operate the airplane above its maximum gross weight.

Aircraft Information

Registration
Make
DIAMOND AIRCRAFT IND INC
Serial Number
40.375
Engine Type
Reciprocating
Year Built
2004
Model / ICAO
DA 40DA40
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
DA 40

Registered Owner (Current)

Name
RRSF LLC
Address
1129 E MAHOGANY LN
City
PLEASANT GROVE
State / Zip Code
UT 84062-2069
Country
United States

Analysis

HISTORY OF FLIGHTOn April 23, 2022, about 1848 mountain daylight time, a Diamond Aircraft DA 40, N321PF, was destroyed when it was involved in an accident near Cedar City Regional Airport (CDC), Cedar City, Utah. The pilot and three passengers were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The operator reported that the pilot rented the airplane with the intent to fly a multileg cross-county flight from his home base of Spanish Fork Municipal Airport/Woodhouse Field (SPK), Spanish Fork, Utah. The planned route of flight comprised stops at CDC and four other airports before returning to SPK. The operator stated that the airplane departed SPK on the first leg with about 40 gallons of fuel.

Recorded airport surveillance video at CDC showed that the accident airplane landed at 1615 and taxied to the self-serve fuel pumps. The pilot and passengers disembarked, and the pilot refueled the airplane, adding about 14 gallons of fuel. The pilot and passengers subsequently boarded the airplane for the next destination, Bryce Canyon Airport (BCE), Bryce Canyon City, Utah, and taxied toward the runway.

A pilot-rated witness, who was driving westbound down Cedar Canyon, reported that he observed the accident airplane flying up the canyon and over the river at an altitude of about 300 ft above ground level (agl). The witness stated that. as the airplane was about to pass over his position, the airplane turned left and then right, and its maneuvers were “quick” and “like a rocking motion.” The witness added that the propeller appeared to be under power and not windmilling.

Another witness, who was traveling near the accident site, reported that he observed the accident airplane flying on an easterly heading over the highway at an altitude of about 200 to 300 ft (agl). The witness stated that, other than being low, the airplane did not appear to be in distress. The witness also stated that that his vehicle’s windows were up, so he could not hear the airplane’s engine. After the airplane passed over the witness’ position, he looked in the mirror and saw the airplane “bank really hard to the south, back across the highway” as if the airplane “were trying to turn around in the narrow canyon.” The witness added that, at that point, the airplane’s wings were “almost completely vertical” and that the airplane “didn’t look like it had enough speed to pull off that maneuver.”

The airplane impacted mountainous terrain along the southern edge of the canyon about 7 miles southeast of CDC. A postcrash fire ensued. PERSONNEL INFORMATIONDuring his last Federal Aviation Administration medical examination, the pilot reported that he was 74 inches tall and weighed 215 pounds. AIRCRAFT INFORMATIONThe weight of the airplane at the time of departure from CDC was estimated to be about 128 pounds over the maximum gross weight (2,646 pounds). Based on the airplane’s most recent weight and balance information, full fuel level (40 gallons), the reported or measured occupant weights, and no baggage. The airplane’s center of gravity (CG) was calculated using the passenger and seat locations in the most favorable position and was found to be outside of the manufacturer’s approved CG envelope.

According to the performance information in the DA-40 Airplane Flight Manual and the assumed altitude and air density conditions, the airplane’s climb performance would have been about 300 ft per minute. METEOROLOGICAL INFORMATIONThe calculated density altitude at the time of departure was about 6,022 ft. The calculated density altitude at the accident location and the time of the accident was 7,203 ft. AIRPORT INFORMATIONThe weight of the airplane at the time of departure from CDC was estimated to be about 128 pounds over the maximum gross weight (2,646 pounds). Based on the airplane’s most recent weight and balance information, full fuel level (40 gallons), the reported or measured occupant weights, and no baggage. The airplane’s center of gravity (CG) was calculated using the passenger and seat locations in the most favorable position and was found to be outside of the manufacturer’s approved CG envelope.

According to the performance information in the DA-40 Airplane Flight Manual and the assumed altitude and air density conditions, the airplane’s climb performance would have been about 300 ft per minute. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed that the airplane impacted mountainous terrain along the southern edge of a canyon about 7 miles southeast of CDC. The airplane came to rest inverted on a magnetic heading of about 289° and at an elevation of 6,583 ft mean sea level. The first identified point of contact (FIPC) was a tall tree with damaged limbs near the top of the tree. The debris path was oriented on a magnetic heading of about 294° and was about 150 ft in length from the FIPC to the main wreckage. All major structural components of the airplane were located in the debris path. The figure below shows the wreckage at the accident site.

Figure. Accident site diagram.

Flight control continuity was established from the cockpit to all primary flight controls. Numerous separations were noted within the flight control system with signatures consistent with overload separation or due to the recovery process. Postaccident examination of the airframe and engine revealed no evidence of mechanical anomalies that would have precluded normal operation. MEDICAL AND PATHOLOGICAL INFORMATIONThe Utah Department of Health, Office of the Medical Examiner, Taylorsville, Utah, performed an autopsy of the pilot. His cause of death was blunt force injuries.

Toxicology testing performed at the Federal Aviation Administration Forensic Sciences Laboratory found no ethanol or drugs of abuse in the pilot’s specimens.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR22FA164