N619AC

Substantial
None

CESSNA 421CS/N: 421C0336

Accident Details

Date
Sunday, May 15, 2022
NTSB Number
CEN22LA202
Location
Monroe, LA
Event ID
20220516105086
Coordinates
32.586050, -91.931094
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
6
Total Aboard
6

Probable Cause and Findings

The failure of the maintenance personnel to properly reinstall the elevator trim tab hardware, which resulted in an in-flight separation of the elevator.

Aircraft Information

Registration
Make
CESSNA
Serial Number
421C0336
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
421CC421
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
8
FAA Model
421C

Registered Owner (Current)

Name
FEED YARD INDUSTRIAL SOLUTIONS LLC
Address
120 SW 6TH AVE
City
AMARILLO
State / Zip Code
TX 79101-2302
Country
United States

Analysis

On May 15, 2022, about 1320 central daylight time, a Cessna 421C, N619AC, was substantially damaged when it was involved in an accident near Monroe, Louisiana. The pilot and five passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot stated that immediately after departure from Morehouse Memorial Airport (BQP), Bastrop, Louisiana, he heard a loud pop and the control yoke oscillated violently. He declared an emergency and diverted to Monroe Regional Airport (MLU), Monroe, Louisiana, about 16 miles southwest, for a longer runway and emergency services. The control yoke and airplane continued to oscillate until the airplane was on final approach, about 3 miles from MLU, then the oscillation stopped. The pilot landed the airplane without further incident.

A postaccident examination of the airplane revealed that the right elevator had mostly separated from the horizontal stabilizer and only a small portion of the inboard elevator remained attached. There was a small puncture on the right side of the rudder.

The elevator trim push-pull rube remained attached to the trim actuator; however, there was no bolt, nut, or cotter pin attached to the aft fork connection, and the trim tab was missing. The push-pull tube did not exhibit any preaccident damage or anomalies. The remainder of right elevator and trim tab were not located.

A review of the airplane’s maintenance logbooks revealed that the elevator trim system was re-rigged on May 13, 2022, two days before the accident. The maintenance personnel who completed the work and signed off on the logbook stated that he did not ensure that the push-pull tube hardware was reinstalled. He added that he checked everything else but missed that step. The airplane had accumulated about 4 hours of flight time since the elevator trim maintenance was completed.

As a result of the accident, the maintenance facility updated their company practices to include a secondary inspection sign-off and updated their work order close out procedures.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA202