N5895Q

Substantial
None

MOONEY M20ES/N: 812

Accident Details

Date
Saturday, June 18, 2022
NTSB Number
CEN22LA255
Location
Stillwater, OK
Event ID
20220621105283
Coordinates
36.172610, -96.959532
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The inadequate maintenance and inspection of the engine induction air coupling, which impeded airflow to the engine and resulted in the subsequent partial loss of engine power.

Aircraft Information

Registration
N5895Q
Make
MOONEY
Serial Number
812
Engine Type
Reciprocating
Year Built
1965
Model / ICAO
M20EM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
349 WOLFE FIELD RD
Status
Deregistered
City
ROGERS
State / Zip Code
TX 76569-3901
Country
United States

Analysis

On June 18, 2022, about 0945 central daylight time, a Mooney M20E airplane, N5895Q, sustained substantial damage when it was involved in an accident near Stillwater, Oklahoma. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The pilot reported that, about 20 to 25 minutes after departure and while in cruise flight at an altitude of about 4,500 ft mean sea level, the airplane lost partial engine power. The power had been set to 2,400 rpm and 24 inches of manifold pressure, which decreased to 2,000 rpm and between 11 and 12 inches of manifold pressure. The pilot manipulated the throttle control, but the engine did not respond. He moved the fuel selector through all positions while also moving the throttle, but the engine still did not respond. Because the airplane was unable to maintain level flight, the pilot elected to conduct a forced landing to a highway. As the airplane was about to land, the pilot became focused on avoiding a vehicle and failed to extend the landing gear. The airplane touched down “very softly” with the gear up, and the pilot turned the airplane slightly to the left to keep the propeller from impacting the vehicle, which resulted in the left wing impacting a road barrier and substantial damage to the wing.

A postaccident examination revealed no anomalies with the engine control system, and throttle control continuity was established from the cockpit controls to the engine. The engine cowling was removed, and the induction air coupling was found wrapped in gray tape (see figure 1). When the tape was removed, separations were visible on the top and bottom at the flange on the inboard side. The inside of the coupling was examined, and the lower portion appeared to be permanently deformed in a manner consistent with compression (see figure 2).

Figure 1. Induction coupling with gray tape.

Figure 2. View from inside the induction coupling

The pilot reported that the airplane’s tachometer time at the time of the accident was about 4,489 hours. According to the maintenance logbooks, the airplane’s most recent annual inspection, in accordance with Title 14 CFR Part 43 Appendix D, was performed on June 11, 2021, at a tachometer time of about 4,429 hours.

The airframe and powerplant mechanic with inspection authorization who completed that annual inspection also completed the airplane’s two previous annual inspections. Those inspections were performed on November 11, 2018, and December 7, 2019, when the airplane’s tachometer time was about 4,380 and 4,396 hours, respectively.

The maintenance entry dated November 11, 2018, noted “installed new Brackett induction air filter.” No other entries in the maintenance logbooks were associated with the induction air filter or coupling. Multiple attempts to contact the mechanic were made with no success. As a result, the investigation could not determine when the tape was applied to the induction coupling.

According to Title 14 Part 43 Appendix D, during an annual inspection, lines, hoses, and clamps should be checked “for leaks, improper condition and looseness” and all systems should be checked for “improper installation, poor general condition, defects, and insecure attachment.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA255