N42WC

Substantial
Minor

ROBINSON HELICOPTER COMPANY R22 MARINERS/N: 1531M

Accident Details

Date
Wednesday, July 27, 2022
NTSB Number
ERA22LA340
Location
Hollywood, FL
Event ID
20220727105598
Coordinates
26.001222, -80.240722
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
1
Total Aboard
2

Probable Cause and Findings

Inadequate maintenance of the helicopter’s tail rotor blades, which resulted in a failure of the tail rotor drive system, and an inflight loss of yaw control from which the flight instructor was unable to recover.

Aircraft Information

Registration
Make
ROBINSON HELICOPTER COMPANY
Serial Number
1531M
Engine Type
Reciprocating
Year Built
1990
Model / ICAO
R22 MARINERR22
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
R22 MARINER

Registered Owner (Current)

Name
N42WC LLC
Address
6 SHEFFIELD RD HNGR 1
City
REHOBOTH BEACH
State / Zip Code
DE 19971-1400
Country
United States

Analysis

On July 27, 2022, about 1345 eastern daylight time, a Robinson R22 helicopter, N42WC, was substantially damaged when it was involved in an accident near Hollywood, Florida. The flight instructor was not injured, and the student pilot received minor injuries. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the instructor, after completing an engine run-up, he “picked up” the helicopter and was air-taxiing to the practice area to conduct some hover work. Before reaching the practice area, a “popping” and “banging” sound was heard from behind the helicopter, followed by an uncommanded right yaw. The instructor attempted to regain control, but the helicopter collided with the ground and rolled over onto its right side. The instructor and student pilot exited the helicopter.

Examination of the helicopter by a Federal Aviation Administration inspector revealed that the tail rotor assembly was separated; both tail rotor blades remained attached and the output shaft was also attached. Both tail rotor blades were bent and were impact damaged. The tail rotor gearbox was fractured, with half of the casing missing. The main rotor blades were bent down and curled, with multiple kinks and creasing from leading edge to trailing edge. Multiple impact signatures were noted on the ground within the rotor diameter of the helicopter.

Examination of the tail rotor gear box and tail rotor blades revealed corrosion within both blades. The exam revealed that erosion of the leading edge provided a path for moisture to ingress into the bond joint and deteriorate the adhesive.

The owner and the mechanic stated that the helicopter’s maintenance records were previously damaged by water and had to be reconstructed digitally. The records provided appeared to show that most life-limited parts had been overflown by 374.1 hours. The pilot stated that he had noted damage on the helicopter’s tail rotor blades during a preflight inspection about two weeks before the accident and that the operator had replaced the blades. Review of the available maintenance records for the helicopter revealed that the serial numbers of the tail rotor blades installed did not match that noted in the maintenance records. The available records also did not document any replacement of the tail rotor blades.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA22LA340