N55338

Substantial
None

PIPER PA-28-140S/N: 28-7325370

Accident Details

Date
Wednesday, August 10, 2022
NTSB Number
CEN22LA385
Location
Sparta, MI
Event ID
20220815105735
Coordinates
43.129510, -85.679470
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The pilot’s delayed decision to reject the takeoff, resulting in a runway excursion and impact with a fence.

Aircraft Information

Registration
Make
PIPER
Serial Number
28-7325370
Engine Type
Reciprocating
Year Built
1973
Model / ICAO
PA-28-140P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
PA-28-140

Registered Owner (Current)

Name
PT ARTS LLC
Address
2450 RAYMOND AVE SE
City
GRAND RAPIDS
State / Zip Code
MI 49507-3924
Country
United States

Analysis

On August 10, 2022, about 1030 eastern daylight time, a Piper PA-28-140 airplane, N55338, was substantially damaged when it was involved in an accident near Sparta, Michigan. The pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that after liftoff, the airplane did not seem to be accelerating. She pushed the nose down to accelerate in ground effect; however, the airplane was approaching the end of the runway and, in her judgement, may not have had sufficient altitude to clear a line of trees. The pilot decided to reject the takeoff. After touching down, she “immediately” applied full brakes but was unable to stop before the airplane departed the runway pavement. It continued into the grass and impacted the airport perimeter fence. The airframe sustained damage to the right wing during the impact.

A postaccident engine examination did not reveal any anomalies consistent with an inability to produce rated power. In addition, the pilot stated that there was no mechanical failure or malfunction associated with the airplane. She noted that factors adversely affecting airplane takeoff performance were density altitude, airplane gross weight, an upsloping runway, and the additional altitude required to clear the tree line.

The preflight weight and balance calculation provided by the pilot indicated a gross takeoff weight of 2,072 lbs and a center-of-gravity location of 90.405 inches. This was within the allowable loading envelope for the airplane. At the time of the accident, the calculated density altitude was about 1,674 ft. Airplane performance data indicated the expected takeoff performance was about 900 ft ground roll, 2,000 ft required to clear a 50-foot obstacle, and an initial climb rate of 550 feet per minute.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA385