N1576F

Substantial
None

MD HELICOPTERS INC 369ES/N: 0568E

Accident Details

Date
Tuesday, August 30, 2022
NTSB Number
CEN22LA402
Location
Pearland, TX
Event ID
20220830105830
Coordinates
29.521278, -95.242139
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot receiving instruction’s failure to maintain aircraft control, and the flight instructor’s delayed remedial action, which resulted in a hard landing.

Aircraft Information

Registration
Make
MD HELICOPTERS INC
Serial Number
0568E
Engine Type
Turbo-shaft
Year Built
2006
Model / ICAO
369E
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
369E

Registered Owner (Current)

Name
CITY OF HOUSTON POLICE DEPT
Address
8402 LARSON HOBBY AIRPORT
City
HOUSTON
State / Zip Code
TX 77061-4107
Country
United States

Analysis

On August 29, 2022, about 2155 central daylight time, an MD Helicopters 369E, N1576F, was substantially damaged when it was involved in an accident at the William P. Hobby Airport, Houston, TX. The flight instructor and pilot receiving instruction were not injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. The flight was conducted by a flight instructor and a commercial pilot who was receiving instruction.

The fight instructor reported that he and the pilot receiving instruction were conducting a simulated power recovery autorotation with a 90° turn. The maneuver was started at 800 ft above ground level (agl) and between 75 and 80 knots (kts) airspeed, and the instructor stated that he was commanding the throttle while the pilot receiving instruction commanded the cyclic, anti-torque, and collective controls. The instructor reduced the throttle and the pilot receiving instruction reduced airspeed to about 60-65 kts. When the helicopter descended to 300 ft agl, the flight instructor increased engine throttle and the pilot receiving instruction continued the autorotation, flared, and leveled the helicopter about 10 ft agl. The flight instructor waited for the pilot receiving instruction to increase collective, but he did not feel the collective control move, so he pulled up on the collective, but the helicopter struck the ground before it could ascend. The helicopter then slid to a stop and the flight instructor pulled the emergency fuel cutoff to shut down the engine. After exiting the helicopter, the instructor saw that the tail boom had separated from the helicopter.

The pilot receiving instruction reported that he had set the helicopter up for a simulated autorotation with a 90° turn and power recovery. He counted down from 3 to begin the autorotation. The throttle was rolled to idle, and the pilot receiving instruction lowered the collective and depressed right pedal. He pitched the helicopter to maintain 60 kts while making a 90° turn to align with the runway. He maintained rotor speed by slightly raising and lowering the collective control. As the helicopter descended through about 150 ft agl, he began to flare. He felt the throttle increase but did not feel the power increase like he had felt on previous autorotations. The helicopter sank fast and struck the runway, skidding to a stop. He noted that the flight instructor pulled the fuel cutoff to stop the engine.

Examination of the helicopter and a subsequent engine test run in a test cell did not reveal any anomalies that would explain a loss of engine power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN22LA402