Accident Details
Probable Cause and Findings
The pilot’s loss of airplane control due to spatial disorientation during initial climb in dark night and low instrument meteorological conditions, which resulted in a descent into terrain. Contributing to the accident was the pilot’s fatigue due to a long day of flying and personal activities.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On October 1, 2022, at 2317 central daylight time, a Cessna 172S, N262TA, was substantially damaged when it was involved in an accident near Hermantown, Minnesota. The commercial pilot and two passengers sustained fatal injuries and two people occupying a house sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot and the two passengers departed South St. Paul Municipal Airport-Richard E Fleming Field (SGS), South St. Paul, Minnesota, about 1015, and had flown to Duluth International Airport (DLH), Duluth, Minnesota, earlier that day to attend a wedding. According to airport security video, the pilot and the two passengers returned to DHL and the pilot conducted a preflight inspection of the airplane at 2246, and the passengers boarded about 2254.
At 2305, the pilot contacted air traffic control and received an instrument flight rules (IFR) clearance back to SGS. A controller cleared the pilot direct to SGS and directed him to climb to 6,000 ft mean sea level (msl). The pilot was also provided a departure frequency and transponder code. The pilot then read back the wrong departure frequency and no beacon code. The controller again provided the beacon code and advised the pilot the rest of the readback was correct, but did not correct the readback of the incorrect departure frequency. The pilot was cleared to taxi to runway 09, during which time the controller informed him that the visibility was about ½-mile. The controller also advised the pilot that after he departed he may be operating in instrument meteorological conditions for a while. This was based on information provided by a King Air pilot who recently departed and reported that the cloud base was about 250 ft above ground level, and that he was still climbing through the clouds at 12,000 ft msl.
The pilot contacted the air traffic control when he was holding short of the runway and ready for takeoff, and the tower controller cleared the pilot for takeoff and to make a right turn direct to SGS. The tower controller also reported that the wind was from 090° at 14 knots gusting to 18 knots, and the runway visual range was greater than 6,000 ft, which the pilot acknowledged.
The rear-seat passenger recorded two brief videos of the takeoff with their mobile phone. The videos were sent to the National Transportation Safety Board recorders laboratory for examination. The videos revealed the airplane’s takeoff and initial climb through 1,500 ft msl. The interior windows were covered with condensation. The instrument panel was visible, and no abnormalities were noted. The takeoff roll and engine sounds appeared normal. The initial climb showed the airplane entering the clouds about 19 seconds after the video began with the takeoff roll. The video was stopped at 24 seconds.
A review of ADS-B data revealed the airplane departed at 2312. It made a right turn toward the south while climbing to about 1,750 ft msl. The airplane then made a steep left turn to a track of about 270° while climbing to 2,800 ft msl before it began to descend (see figures 1 and 2).
Figure 1 - ADS-B data depicting an orthogonal plot of the airplane’s flight track in profile in red.
Figure 2 – Overhead plot of the airplane’s flight track with points depicting the airplane’s position, altitude, and time annotated.
The radar controller attempted to contact the pilot on the departure frequency with no response. The radar controller then transmitted on the tower frequency and instructed the pilot to contact departure. The pilot responded by saying “contacting departure two tango alpha.” Several seconds later, while the airplane continued to descend in a counterclockwise direction and increasing in ground speed, the radar controller advised the pilot that he observed the airplane descending and asked the pilot to confirm he was climbing. There was no response. Simultaneously, there was a low altitude alert observed on the control tower display workstation. Both the tower and radar controllers continued with repeated attempts to contact the pilot but received no response.
PILOT INFORMATION
The pilot held a commercial pilot certificate with ratings for airplane single-engine land and instrument airplane. He was also held a flight instructor certificate with an airplane single-engine rating. A review of the pilot’s logbook revealed he had accumulated 645.9 total hours of flight experience, of which 39.9 hours were in the accident airplane make and model. His total nighttime flight experience was 45.1 hours, of which 2.5 hours were in the accident airplane make and model. His flight time in actual instrument meteorological conditions was 7.6 hours, of which 1.5 hours were in the accident airplane make and model. His most recent actual instrument flight experience was in July 2021, about 15 months before the accident flight and his most recent simulated instrument experience was 2.5 hours in June 2022.
METEOROLOGICAL INFORMATION
The weather conditions at DLH at 2255 was reported as wind from 080° at 10 knots, gusting to 19 knots, visibility 5 miles in mist, an overcast ceiling at 200 ft agl, a temperature of 9° C, a dew point of 8° C, and an altimeter setting of 30.38 inHg.
At 2355, the weather was reported as wind from 080° at 12 knots, visibility 4 miles in mist, an overcast ceiling at 200 ft agl, a temperature of 9° C, a dew point of 8° C, and an altimeter setting of 30.38 inHg.
The National Weather Service reported that between the hours of 1855 through 0155, low IFR (LIFR) conditions would prevail. Per the Federal Aviation Administration (FAA) Aeronautical Information Manual, section 7-1-7, LIFR was defined as the ceiling or the lowest layer of clouds reported as broken or overcast, or the vertical visibility into a surface-based obscuration below 500 ft above ground level (agl) and/or visibility less than 1 statute mile.
WRECKAGE INFORMATION
The airplane impacted electrical transmission wires and a 2-story home. The wing and left landing gear imprint on the house were consistent with the airplane impacting it in a 40° left bank as the airplane passed through the structure. It passed through two upstairs bedrooms as the occupants of the house slept, and then exited the home and came to rest inverted between a vehicle and a detached garage. There was no post-impact fire. The wreckage path was oriented on a magnetic heading of 205° and was about 175 ft in length. All major components of the airplane were located within the wreckage site.
Figure 3 - Aerial photograph of the accident site including the damaged house and the debris field that extended beyond it (photo courtesy of the Hermantown Police Department)
The left wing was impact separated from the fuselage and came to rest in the front yard of the house. The empennage was separated from the fuselage at the leading edge of the horizontal stabilizer and was discovered against the front door of the detached garage. The remaining fuselage, cockpit, and right wing were inverted and wedged between the garage and a vehicle. No visible fuel was present at the scene and there was no associated fuel blight discovered on the trees or surrounding grass; however, fire rescue personnel reported a strong fuel odor during their recovery operations shortly after the accident.
Control continuity was confirmed from all flight control surfaces through breaks in the flight control cables that were consistent with tensile overload.
The engine was impact separated from the firewall and remained upright adjacent to the fuselage. The engine had impact damage to various pushrods, intake and exhaust tubes, rocker box covers, and cylinder No. 2 cooling fins. The propeller flange was sheared off at the crankshaft and the damage was consistent with rotation of the crankshaft at the time of impact. The propeller was found in the wreckage next to the engine and exhibited chordwise scraping and leading-edge gouges. Both propeller blades were bent aft mid-span and the propeller spinner was crushed and twisted.
The engine spark plugs were removed and examined. They had minimal wear when compared to the Champion Check-A-Plug chart. Both the left and right magnetos were intact. Both units were operated manually with a drill and all posts produced a spark with no anomalous behavior noted. Residual fuel was discovered in the fuel pump and fuel odor was noted in the flow divider.
The engine was rotated via the accessory section. Thumb compression and suction was attained on all cylinders and crankshaft continuity was confirmed. The crankshaft rotation was smooth, with no noticeable abnormal noise or friction noted and all internal components appeared well lubricated. Each cylinder was inspected internally with a lighted borescope, and no mechanical issues were observed.
The attitude indicator, heading indicator, and turn coordinator were examined. The gyros were capable of smooth rotation and rotational scoring was noted on the electrically-powered turn coordinator gyro. There was no rotational scoring noted on the vacuum-driven attitude indicator gyro or heading indicator gyro. The vacuum manifold was examined, and the diaphragms displayed normal operating signatures. All air tubes/manifolds were free of obstructions and the vacuum pumps were intact and capable of expelling air when rotated by hand. Each pump displayed normal operating signatures and continuity of the pump, and tubes to their respective instrument was confirmed.
There were 3 on-board data units that were retained and sent to the NTSB recorders lab for examination and download: an Appareo Stratus 2S, a Garmin GTN 750, and a DAC International GDC31. The data extracted from the Stratus included sessions from September 13, 2022, through September 28, 2022, and no data associated with the accident flight were recorded on the device. The Garmin GTN 750 sustained impact damage that prevented the device from being ...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23FA001