N7254L

Substantial
None

AMERICAN AVIATION AA-1AS/N: AA1A-0454

Accident Details

Date
Friday, November 4, 2022
NTSB Number
ERA23LA059
Location
Sparta, TN
Event ID
20221115106295
Coordinates
36.056738, -85.530106
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power due to an accumulation of carburetor ice, resulting in an off-airport landing and substantial damage to the airplane.

Aircraft Information

Registration
N7254L
Make
AMERICAN AVIATION
Serial Number
AA1A-0454
Engine Type
Reciprocating
Year Built
1972
Model / ICAO
AA-1AAEA1
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
6000 DOUGLAS DR N
Status
Deregistered
City
CRYSTAL
State / Zip Code
MN 55429-2314
Country
United States

Analysis

On November 4, 2022, about 1715 central standard time, an American Aviation AA-1A, N7254L, was substantially damaged when it was involved in an accident near Sparta, Tennessee. The private pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 test flight.

The pilot stated that, during an annual inspection the day before, he had discovered and repaired an irregularity with an air intake hose. The accident flight was a post-maintenance test flight. He performed a thorough preflight inspection and engine run-up before takeoff with no anomalies observed.

Shortly after takeoff, the pilot climbed the airplane to about 6,800 ft mean sea level (msl) while conducting rectangular patterns directly over the airport, then initiated a descent to 4,500 ft msl. During the descent, without any warning, the airplane “completely” lost all engine power. The pilot reported that he never reduced power during the descent; he maintained takeoff power or cruise power for the entire duration of flight, even during the descent.

The pilot’s attempts to restart the engine were unsuccessful. As the airplane continued to descend, he approached the airport on the downwind leg of the traffic pattern abeam the runway 22 numbers at 4,000 ft msl (2,075 above ground level). The pilot decided the airplane was too high to land on the runway and he conducted a slip to lose altitude. Upon completion of the slip, the pilot realized he had over-corrected and was too low to reach the runway. He elected to perform a forced landing in a field about 1/2 mile before the runway. The pilot flew below powerlines and landed hard on rough, hilly terrain. The airplane impacted a fence and brush before coming to rest.

Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that the left and right wings were crushed at multiple locations, and the fuselage was buckled under the engine compartment. A subsequent examination by the FAA inspector and a mechanic revealed that the engine air inlet was packed with dirt, but the induction system components were otherwise intact and not obstructed. The carburetor heat butterfly valve was in the open (cold) position, fuel was present in the carburetor and the fuel pumps operated and showed no anomalous behavior. Engine crankshaft continuity was established, and the spark plugs showed normal coloration.

The recorded temperature and dew point near the accident site was about 71°F and 50°F, respectively. On the carburetor icing probability chart, those temperatures were in the “serious icing – glide-power” range; however, at altitude about 6,000 ft msl, near where the loss of engine power occurred, weather sounding data revealed temperature and dewpoint was about 49°F and 35°F, respectively, which bordered on the serious icing at a cruise power setting.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23LA059