Accident Details
Probable Cause and Findings
The pilot’s failure to maintain airplane control while landing with a left gusting crosswind. Contributing to the accident was the partial loss of engine power during the go-around.
Aircraft Information
Registered Owner (Current)
Analysis
On May 1, 2023, at about 1345 central daylight time, a Cessna 182D, N8713X, was substantially damaged when it was involved in an accident near Batesville, Mississippi. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot reported that he was making a planned fuel stop at Panola County Airport, Batesville, Mississippi (PMU), when he experienced moderate to heavy “wind chop” as he approached the airport. The pilot’s first approach was too high, so he conducted a normal go-around and re-entered the traffic pattern. During the second approach, he used no flaps; the airplane bounced and was pushed to the right by a “significant” wind gust. The pilot attempted a go-around by adding full power; the engine rpm increased, but then he heard a “pop” and the engine lost power. The airplane landed in the grass next to the runway; however, after touchdown, the pilot was unable to stop the airplane before it hit a drainage ditch with the left main wheel, which resulted in the left wheel separating from the strut and substantial damage to the lower fuselage. The airplane’s right wing subsequently impacted the ground, resulting in substantial damage to the wing.
A review of video taken of the approach and attempted go-around revealed that the airplane bounced on the runway and settled back down to the right. As it exited the paved surface, the engine rpm increased, and the airplane became airborne again. Then the engine sputtered and lost power and the airplane touched down in the grass, bounced, and touched down again on the taxiway. The airplane bounced once more before impacting the drainage ditch.
A postaccident examination did not reveal any preimpact mechanical malfunctions or failures that would have precluded normal operation. The wings and empennage had been removed for transport. The right fuel tank finger screen was examined and was not obstructed. The left-wing fuel pickup screen was damaged during the recovery; however, it was not obstructed. The engine remained attached to the fuselage. The propeller remained attached to the hub. Both propeller blades were bent aft about 45° and exhibited chordwise scratching.
A postaccident engine run took place on June 7, 2023. Fuel was supplied from an external fuel tank and plumbed into the engine from the right-wing-root fuel pickup. The engine started, idled, and accelerated without hesitation. The engine was shut down and no anomalies were noted during the engine run. Fuel was then supplied from an external fuel tank and plumbed into the left-wing-root fuel pickup and performed similarly to the previous engine run: started, idled, and accelerated without hesitation.
Although the weather conditions at the time of the accident were conducive to the accumulation of carburetor icing at glide power, the pilot reported that he used carburetor heat during the two landing approaches.
Wind at the time of the accident was from 290° at 10 knots gusting to 21 knots; the calculated crosswind was about 20 knots. The pilot was landing on runway 01. While the pilot operating handbook for the 182D did not list a maximum demonstrated crosswind component, later models listed a 15 knot crosswind for landing and a 20 knot crosswind for takeoff.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN23LA168