Accident Details
Probable Cause and Findings
A No. 2 (right) engine failure due to a spinner fairing separation and subsequent impact with the fan blades that resulted in a midspan fracture of one fan blade. The spinner fairing separated as a result of a fatigue crack that originated from the heat affected zone of a tack weld that secured a spacer to the aft side of the fairing. Contributing to the incident was inadequate spinner fairing inspection procedures that did not require removal of the spinner fairing to inspect the aft side for earlier detection of crack indications.
Aircraft Information
Registered Owner (Current)
Analysis
History of Flight
On June 17, 2023, about 1059 central daylight time (CDT), a Gulfstream G-IV, N926TT, equipped with two Rolls-Royce Tay 611-8 turbofan engines, operated by Planet 9 Private Air, LLC, experienced a No. 2 (right) engine failure shortly after beginning a step climb at FL400. The flight crew secured the No. 2 engine, declared an emergency, and diverted the airplane to Sioux Gateway Airport (SUX), Sioux City, Iowa where they made an uneventful single engine landing. There were no injuries reported. The airplane was operated as a Title 14 Code of Federal Regulations Part 135 flight from Philadelphia International Airport (PHL), Philadelphia, Pennsylvania to Charles M. Schulz Sonoma County Airport (STS), Santa Rosa, California.
Damage to the Airplane
There were multiple small impacts on the right wing that extended up to approximately 60 inches forward of the No. 2 engine inlet cowl leading edge lip. One impact on the right wing flap penetrated the wing skin. Additional small impact marks were observed on fuselage inboard of the engine, on the aft right window, and on the leading edge of the right horizontal stabilizer.
Test And Research
No. 2 Engine Nacelle Examination
The No. 2 engine inlet cowl had multiple acoustic liner impact gouges into the honeycomb structure, 360 degrees around the circumference. The impact damage was most severe from the fan blade path leading edge to approximately 12 inches forward of the fan blades. There was a rounded slice at the 8 o’clock position that had an arc length of approximately 15 inches. The inlet cowl had a penetration at the 1 o’clock position that measured approximately 12 inches circumferentially by 7 inches axially at the widest points. The penetration extended axially from the inlet cowl bulkhead to approximately 2 inches forward of the inlet cowl-to-fan case flange (Photo 1). The inlet cowl composite and metal material around the hole was petaled radially outward. There were two additional small inlet cowl penetrations at the 3 o’clock and 10 o’clock positions. The penetration at the 3 o’clock position measured approximately 0.5 inch axially by 2 inches circumferentially and extended forward from the inlet cowl-to-fan case flange. The fan cowl metal and thermal blanket insulation around the hole were displaced radially outward. The small penetration at the 10 o’clock position was located on the inlet cowl-to-fan case flange. Light was barely visible through the impact and there was no evidence of material escape.
Photo 1- Inlet Cowl Penetration, 1 o'clock Position
No. 2 Engine, Rolls-Royce Tay 611-8, Serial Number, 16870, Examination
The No. 2 engine was removed from the airplane with a forklift crane and placed in a shipping stand for visual examination. There was no evidence of undercowl fire or thermal damage. The fan spinner fairing had separated and was missing. The three fairing attaching bolts had fragments of the fairing still secured under the bolt heads (Photo 2). The fan blades all exhibited leading edge hard body impact damage, tearing, and materials loss along the full blade span (Photo 3). One fan blade, identified as blade position 7 on the blade platform, was separated at the midspan. The released portion of the blade was contained within the fan case and was recovered from the space forward of the fan outlet guide vanes. The fan blade attrition lining had heavy 360 degree rub and impact damage. The ice resistant liner aft of the fan blade plane of rotation also exhibited 360 degree impact damage and was missing material at multiple locations. The visible intermediate pressure compressor (IPC) blades had leading and trailing edge nicks and the blade tips had heavy rub/uneven wear consistent with an impact and operation with a significant out-of-balance.
Photo 2- Spinner Fairing Separated, Fairing Fragments Under Attaching Bolts
Photo 3- Fan Blade Damage, Fan Blade Position 7 Midspan Separation
An anti-ice servo air line b-nut connector was backed off at the 2 o’clock position. Immediately below the backed off b-nut connector, the air line was fractured at the boss weld into the main bleed air duct. The P3 limiter, attached to the fuel flow regulator (FFR) and situated at the 7 o'clock position, was separated at the mating flange. There are three connecting bolts holding the component onto the FFR, two of the bolts were broken and one bolt had backed off. A pressure fuel line off the acceleration reset solenoid was fractured. The fractured line was located at the 8 o’clock position on the bypass case. There was no visual evidence of fuel streaking on the left side of the engine.
Materials Analysis
The recovered spinner fairing attaching hardware including the metal fragments under the attaching bolt heads, all fan blades, and the recovered fan blade position 7 fan blade tip fragments were shipped to the Rolls-Royce Deutschland Ltd. & Co. KG Materials Laboratory in Dahlewitz, Germany for failure analysis.
The Materials Laboratory identified fatigue cracks on two of the three bolt hole fixture pockets that initiated in the heat affected zone of the tack welds that hold the fairing spacer in position. The analysis could not determine if the fatigue mode was high cycle fatigue (HCF) or low cycle fatigue (LCF) and was likely a combination of both. The tack welds on each of the three spinner fairing bolt assemblies were greater than 10mm (millimeters) in length with visually good quality and no evidence of weld voids or other anomalies. Fairing bolt assembly 2, spot weld 2 was sectioned to perform a microscopic examination of the fairing and washer material microstructure. The depth of the weld influence was measured approximately 3.6 mm and the microstructure of both the spinner fairing sheet metal or washer experienced significant grain growth, which was considered typical of a normal weld in this location. Scanning Electron Microscopy using Energy Dispersive X-ray Spectroscopy (SEM/EDS) of the spinner fairing identified it to be consistent with Titanium (Ti) 6/4 as specified in the engineering drawing.
The fracture surfaces of fan blade position 7 were approximately 7.56 inches-8.66 inches (192mm-220mm) above the platform. The fracture surfaces were consistent with forced rupture (overload) originating from a leading edge impact. SEM/EDS analysis confirmed the fan blade material was consistent with Ti 6/4 as specified on the part drawing.
Spinner Fairing Modal Analysis Testing
Modal impact testing (hammer test) was performed on a spinner fairing in multiple configurations with and without fan hub and nose cone attaching hardware. The testing identified that the spinner fairing’s natural frequency is close to a non-integral fan blade vibration mode that is a high altitude speed related excitation and is transmitted to the spinner fairing through pressure fluctuations. Variables that affect the fan blade vibration mode include fan blade leading edge shape, fan pressure ratio, and fan speed. Rolls-Royce operating history has shown that manufacturing variability causes some fan blade sets to excite the spinner fairing 1st natural frequency while others do not.
The testing also identified a fan blade mode that crosses at 70% N1. The 70% N1 crossing is mostly encountered as a transient during acceleration to takeoff power. It can also occur during ground operations in a crosswind, but there is no evidence of dwell during normal engine operation.
Testing and fleet operational history have also shown that the gap between the spinner fairing, and nose cone can also affect the spinner fairing vibratory response. Rolls-Royce released Notice to Operators (NTO) 38, in August 1997, to recommend replacement of the nose cone on engines where spinner fairing cracks were identified. Nose cone replacement has been shown to be effective at detuning spinner fairing vibration. In cases where the nose cone has been replaced, there have been no known further instances of fairing cracking.
Spinner Fairing Inspection
Different variants of the Tay engine are used for corporate operations (e.g., Tay 611-8, on Gulfstream G-IV) and regional operations (e.g., Tay 610-15, on Fokker 100), although they all share similar turbomachinery. For the Gulfstream G-IV/TAY611-8, operated by Planet 9 Private Air, LLC (corporate operations), the spinner fairing inspection interval specific by the aircraft maintenance manual (AMM) is every 2000 hours. For regional operations the interval is every 600 cycles.
According to the engine logbook, the No. 2 engine spinner fairing was inspected by Planet 9 Private Air, LLC on October 12, 2022. The engine had accumulated approximately 542.2 hours since the spinner fairing inspection at the time of the incident event. The AMM procedure applicable at the time of the last inspection was 72-00-00, Engine -Inspection/Check, 1. Spinner Fairing- Detailed Inspection, instructed maintenance technicians to inspect for cracks and indentations emanating from spinner fairing bolt holes. The procedure did not call for removal of the spinner fairing from the nose cone.
According to Rolls-Royce, there have been field findings of spinner fairing cracks that have extended through the sheet metal until visible on the forward side of the fairing. The origin of the spinner fairing cracks in each crack findings to date has been the heat affected zone of the tack welds that secure the spacer to the aft side of the fairing and therefore the early stages of crack progression are only visible if the spinner fairing is removed from the nose cone. It is unknown if the spinner fairing crack on the incident engine had grown to where it would have been visible on the forward side of the fairing during the October 2022 inspection.
Corrective Actions
Rolls-Royce released Notice to Operators (NTO) number 155 on October 20, 2023, for all Tay engines. The NTO provided updated nose cone fairing inspection criteria to the engine maintenance manual...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ENG23LA030