Accident Details
Probable Cause and Findings
The blockage of the left fuel tank vent, which resulted in a total loss of engine power due to fuel starvation. Contributing to the accident of the pilot’s failure to use his checklist to address the loss of engine power.
Aircraft Information
Registered Owner (Current)
Analysis
On July 20, 2023, about 1236 central daylight time, a Beech A36 airplane, N36900, sustained substantial damage when it was involved in an accident near Oberlin, Kansas. The pilot was not injured and the passenger sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
About 0900 mountain daylight time, the airplane departed from Northeast Wyoming Regional Airport (GCC), Gillette, Wyoming, and was en route to Dalhart Municipal Airport (DHT), Dalhart, Texas. The pilot reported that while in cruise flight over a cloud layer near Oberlin, the airplane sustained a loss of engine power as if it were out of fuel. The pilot attempted to restore engine power by switching to the right fuel tank and activating the starter using the ignition key; however, the attempts to restart the engine were unsuccessful. As the airplane descended through the cloud layer, the pilot switched back to the left fuel tank and focused his attention on the airplane instruments to maintain airplane control.
The airplane descended through the clouds and the pilot regained visual ground reference about 1,500 ft above ground level. The pilot maneuvered the airplane for a forced landing to a road. Upon touchdown the right main landing gear traveled onto the shoulder of the road and the airplane exited the road and collided with an embankment. The airplane sustained substantial damage to the left wing and fuselage.
According to the Federal Aviation Administration inspector who responded to the accident, both fuel tanks had visible fuel and both fuel caps were attached and in place.
The pilot reported that the loss of engine power was due to a broken fuel pump shaft. However, during the postaccident examination, the engine-driven fuel pump shaft and drive coupler were found to be intact. The fuel pump was operationally checked and no anomalies or malfunctions were noted with its operation.
The National Transportation Safety Board performed a postaccident examination of the airframe and engine. The examination revealed an obstruction in the left tank fuel vent. The one-way check valve in the fuel vent was observed stuck in the closed position, not allowing air through. When the fuel vent line was pressure tested the obstruction became dislodged. Further examination of the check valve revealed debris inside consistent with insect debris (Figure 1). No other mechanical anomalies were noted during the examination that would have precluded normal operation.
Figure 1: Left tank fuel vent check valve.
The airplane manufacture’s emergency procedures checklist for an air start procedure after an inflight engine failure includes selecting the auxiliary fuel pump ON. The pilot did not engage the auxiliary fuel pump during his restart attempts.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN23LA344