Accident Details
Probable Cause and Findings
A collision with trees during takeoff for reasons that could not be determined based on available information.
Aircraft Information
Analysis
On August 3, 2023, at 0930 eastern daylight time, an unregistered Kolb Firestar was substantially damaged when it was involved in an accident near McAlpin, Florida. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
A witness located along the middle of runway 18 at Little River Airport (FL10), McAlpin, Florida, reported he watched as the accident pilot taxied by his hangar about 0930 and to the end of runway 18 to complete an engine runup and preflight check. He then watched as the pilot started the takeoff roll. As the airplane passed his hangar, he could no longer see the airplane as the hangar was blocking his view. He heard a decrease in engine noise that he attributed to the pilot aborting the takeoff, as if the power was reduced to idle. The witness then went inside his house for a few minutes before deciding to drive down the runway and see if the pilot needed any help. He drove down to the end of runway 18 but did not see the pilot or the airplane.
Later in the evening, around 1800, he heard from other neighbors that the pilot and airplane were missing. He drove down the runway again to look for the airplane but did not see anything. Around 2000, he walked down the runway again and looked into the tree line. After walking into the woods, he located the airplane suspended about 50 ft above him in the treetops and the deceased pilot was lying on the ground next to a tree.
The accident site was in a wooded area, displaced laterally about 50 ft from the middle of runway 18. The airplane was inverted and hanging from the left main landing gear. The airplane was lowered to the ground and 4 ft of the left outer wing and the rudder were impact damaged. The right wing’s fabric was torn. The engine and cabin section were intact and unremarkable. The propeller was unremarkable. The pilot’s 4-point restraint was unlatched. An engine test run was conducted and the engine started immediately when the key was turned to the start position. The engine ran smoothly and ran up to high rpm without any hesitation or any anomalies noted. Flight control continuity was established from all flight control surfaces to the flight controls in the cockpit.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA23FA321