N90HM

Substantial
None

MAGNI M24S/N: 24169824

Accident Details

Date
Monday, October 16, 2023
NTSB Number
CEN24LA013
Location
Mount Sterling, IL
Event ID
20231016193246
Coordinates
39.986285, -90.803982
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s failure to maintain gyroplane control on the downwind leg, which resulted in impact with terrain. Contributing to the accident was the pilot’s distraction.

Aircraft Information

Registration
Make
MAGNI
Serial Number
24169824
Engine Type
Reciprocating
Year Built
2020
Model / ICAO
M24MM24
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
MAGNI M-24

Registered Owner (Current)

Name
PEACOCK ROBERT W
Address
1697 ORE RD
City
CHAPIN
State / Zip Code
IL 62628-4118
Country
United States

Analysis

On October 16, 2023, about 1130 central daylight time, a Magni M24 gyroplane, N90HM, was substantially damaged when it was involved in an accident near Mount Sterling, Illinois. The pilot was not injured. The gyroplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The pilot reported that the gyroplane was on downwind for runway 36 at the Mount Sterling Municipal Airport (I63), when he noticed that his airspeed had decayed to 37 mph, below the recommended traffic pattern airspeed of 65 mph. He reported that his airspeed had decayed while his attention was diverted looking for other traffic. The pilot attempted to correct by increasing engine throttle but subsequently lost control. The gyroplane impacted terrain in the left downwind, which resulted in substantial damage to the main rotor system and empennage.

During the recovery of the gyroplane, the smell of automotive fuel was present with soil discoloration around the area of the fuel cap. Postaccident examination revealed no preaccident mechanical failures or malfunctions with the gyroplane that would have precluded normal operation. The engine was successfully operated during the examination.

The rotor pitch trim actuator arm was observed to be 2 inches from the actuator, which corresponds to a pitch trim setting of about 65 mph. The gyroplane flight manual recommends an airspeed of 65 mph during the traffic pattern when preparing to land.

The FAA Rotorcraft Flying Handbook (FAA-H-8083-21), Section 21-3, states that, “If rotor force is rapidly removed, some gyroplanes have a tendency to pitch forward abruptly. This is often referred to as a forward tumble, buntover, or power pushover.” Referring to the recovery procedure, it notes that, “In most cases, you need to remove power and load the rotor blades.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN24LA013