N118PW

Substantial
None

AERO COMMANDER 500-BS/N: 1460-163

Accident Details

Date
Tuesday, November 7, 2023
NTSB Number
CEN24LA033
Location
Jackson, MI
Event ID
20231108193361
Coordinates
42.245777, -84.405968
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power to both engines as a result of the pilot’s improper fuel management. Contributing was the inoperative fuel quantity sending unit.

Aircraft Information

Registration
Make
AERO COMMANDER
Serial Number
1460-163
Engine Type
Reciprocating
Year Built
1964
Model / ICAO
500-BAC50
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
7
FAA Model
500-B

Registered Owner (Current)

Name
CENTRAL AIRLINES INC
Address
4002 W 57 ST
City
FAIRWAY
State / Zip Code
KS 66205
Country
United States

Analysis

On November 7, 2023, at 1510 eastern standard time, an Aero Commander 500B, N118PW, was substantially damaged when it was involved in an accident near Jackson, Michigan. The pilot was uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 positioning flight.

The pilot stated that, about 30 minutes after departure, he began to observe “erratic/low fuel pressure” on the right engine. The pilot descended the airplane from 7,000 ft to 5,500 ft, reduced engine power, and turned the fuel boost pump on. Upon reaching 5,500 ft, fuel pressure returned to normal, and the engine produced full power. About 15 to 20 minutes later, the same engine and fuel pressure symptoms reoccurred and the pilot reduced engine power, turned the fuel boost pump on again, descended the airplane to 3,500 ft, and engine power and fuel pressure were restored. About 15 miles from the destination airport, the fuel pressure to the right engine was lost, and the right engine began surging and producing partial power. Shortly thereafter, left engine fuel pressure was lost and both engines were producing partial power: between 12 to 15 inches manifold pressure and less than 10 psi of fuel pressure. The airplane could not sustain level flight, and the pilot performed a forced landing to a field, during which the airplane sustained substantial damage to the left wing.

During an initial postaccident examination of the airplane, only residual fuel was drained from the fuel system. A security seal was not placed over the fuel tank filler port(s), and the airplane was in the field and unmonitored until an engine run, and a subsequent airplane examination was performed on November 29, 2023at the accident site. The subsequent examination of the fuel system, which included the airframe fuel filters and flow dividers, did not reveal any debris or contaminants. About 27 gallons of 100 low lead aviation fuel was drained from the airplane after the airplane was leveled using jacks. The fuel drained did not contain contaminants. About 6 gallons of fuel was added to the fuel system; both engines started and ran without any anomalies that would have precluded normal operation. Testing of the fuel quantity sending unit, The Liquidometer Corp. part number EA515B-1404M, indicated full at varying levels and down to an empty level of actual fuel quantity.

Bench testing of the fuel boost pumps, fuel servos, and the fuel manifold valve assembly with attached lines and fuel nozzles revealed no anomalies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN24LA033