N6126UAIR TRACTOR INC AT-502A2024-01-10 NTSB Accident Report

Substantial
None

AIR TRACTOR INC AT-502AS/N: 502A-0298

Summary

On January 10, 2024, a Air Tractor INC AT-502A (N6126U) was involved in an incident near Stratford, CA. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

On January 10, 2024, about 1010 Pacific standard time, an Air Tractor AT-502A, N6126U, was substantially damaged when it was involved in an accident near Stratford, California. There were no injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 137 agricultural flight. The pilot reported that during takeoff the airplane failed to develop full power. At approximately 200 feet the engine rolled back to near idle. The pilot’s attempt to vary power lever inputs did not affect engine power output. The pilot maneuvered the airplane between two houses into a grove of small trees. The airplane sustained substantial damage to the wings and fuselage. The airplane has been secured for examination.

This incident is documented in NTSB report WPR24LA070. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N6126U.

Accident Details

Date
Wednesday, January 10, 2024
NTSB Number
WPR24LA070
Location
Stratford, CA
Event ID
20240110193638
Coordinates
36.204833, -119.794110
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power due to the malfunction of the engine compressor bleed-off valve.

Aircraft Information

Registration
Make
AIR TRACTOR INC
Serial Number
502A-0298
Engine Type
Turbo-prop
Year Built
1995
Model / ICAO
AT-502AAT5T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
AT-502A

Registered Owner (Current)

Name
R & D LEASING INC
Address
19101 KENT AVE
City
LEMOORE
State / Zip Code
CA 93245-9137
Country
United States

Analysis

On January 10, 2024, about 1010 Pacific standard time, an Air Tractor AT-502A airplane, N6126U, was substantially damaged when it was involved in an accident near Stratford, California. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 positioning flight.

The pilot reported that the airplane was being repositioned to another location to apply fertilizer and that the hopper was empty. During takeoff the airplane failed to develop full power. At about 200 ft agl, the engine rolled back to near idle. The pilot’s attempt to vary power lever inputs did not affect engine power output. Unable to maintain altitude, the pilot maneuvered the airplane between two houses into a grove of small pistachio trees and soft dirt. The gas generator compressor turbine (CT) was still running when the pilot got out of the airplane. He shut off the fuel and secured the engine. The airplane sustained substantial damage to the wings.

The fuel tanks in both wings were breached. Fuel was observed in the surrounding areas under the airplane. Power control continuity was established from the cockpit controls to the engine. The high-pressure pump filter and last-chance filter were removed: visual examination revealed that both contained fuel and were clean. A fuel sample was obtained from the fuel farm and no contaminants were found. The engine was shipped to the engine manufacturer for additional examination and testing. No preaccident mechanical malfunctions or failures with the airframe that would have precluded normal operation were observed.

Examination of the engine at the engine manufacturer’s facilities revealed the power section, of the engine showed buckling and rotational internal contact of the exhaust casing which was consistent with the accident sequence to the power turbine section. An alternate power section was provided by the manufacturer and was installed on the gas turbine section of the engine to facilitate an engine operational check.

The engine was installed in the test cell and started normally. Following a short dwell period at ground idle speed to raise the oil temperature, the engine slowly accelerated to approximately 35,000 rpm (95% Ng). The test cell plenum pressure change confirmed that the compressor bleed-off valve (BOV) closed during engine acceleration. Subsequent review of the data showed the BOV was slow to close. The test cell T5 temperature (inter turbine temperature) readings began to fluctuate, and the engine was shut down for troubleshooting. Engine testing was interrupted due to a slave PS wire harness malfunction and ended to prevent the risk of overtemperature.

Review of the engine run test data and hesitation heard during the engine sweep was consistent with a compressor BOV malfunction. Subsequent bench testing of the BOV revealed air leakage around the piston and P3 feed gasket. Bench test pressure check of the BOV revealed an abnormal amount of air leaking around the piston. Disassembly of the BOV revealed a piston ring set was stuck within the piston groove, consistent with an abnormal air leak and irregular function. Abrasive and adhesive wear was observed on the piston rings and piston groove, consistent with the environmental debris and/or by the twist observed on the BOV metal piston ring.

During the disassembly of the BOV, two assembly part numbers were vibro-peened by hand on the BOV cover, with neither of the two-part numbers having a strike through.

A review of the maintenance records revealed that the BOV had been disassembled, cleaned, inspected and repaired in April of 2012 by Dallas Airmotive, which is a designated overhaul facility for Pratt & Whitney Canada. This BOV was not installed on the engine at delivery.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR24LA070