N729CWBEECH A362024-03-17 NTSB Accident Report

Substantial
None

BEECH A36S/N: E-2390

Summary

On March 17, 2024, a Beech A36 (N729CW) was involved in an incident near Blackshear, GA. All 3 people aboard were uninjured. The aircraft sustained substantial damage.

On March 17, 2024, at 0825 eastern daylight time, a Beech A36 single-engine airplane, N729CW, was substantially damaged when it was involved in an accident near Blackshear, Georgia. The private pilot and the two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The airplane departed Jacksonville International Airport (JAX), Jacksonville, Florida, at 0753, and was destined for Wood County Airport (1G0), Bowling Green, Ohio, on an instrument flight rules (IFR) flight plan. The pilot stated that the airplane was climbing through 11,000 ft mean sea level (msl) to 13,000 ft msl, when he noticed a reduction in engine power and inability to climb.

This incident is documented in NTSB report ERA24LA143. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N729CW.

Accident Details

Date
Sunday, March 17, 2024
NTSB Number
ERA24LA143
Location
Blackshear, GA
Event ID
20240318193952
Coordinates
31.306100, -82.242100
Nearest Airport
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

A catastrophic engine failure due to oil starvation, which resulted in a total loss of engine power.

Aircraft Information

Registration
Make
BEECH
Serial Number
E-2390
Engine Type
Reciprocating
Year Built
1987
Model / ICAO
A36BE36
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
A36

Registered Owner (Current)

Name
WRIGHT MATTHEW J
Address
1103 PEARL ST
City
BOWLING GREEN
State / Zip Code
OH 43402-2663
Country
United States

Analysis

On March 17, 2024, at 0825 eastern daylight time, a Beech A36 airplane, N729CW, was substantially damaged when it was involved in an accident near Blackshear, Georgia. The private pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported a reduction in engine power and an inability to climb as he was ascending through 11,000 ft mean sea level. The pilot observed a loss of oil pressure followed by a rough running engine that eventually seized. The pilot made a forced landing to a rural road and impacted a tree, which resulted in substantial damage to the right wing and engine mounts.

A review of photographs taken by first responders revealed a large amount of residual oil on the inside of the engine cowling. The pilot reported that he checked the oil before departure and added 1 quart of oil to the 11 quarts present, for a total of 12 quarts.

After the accident, the airplane was relocated to a secured facility and the engine and turbocharger were removed from the airframe by salvage personnel and shipped to Continental Aerospace Technologies, Mobile, Alabama, for further examination. The mechanic who removed the turbocharger reported there were no loose fittings or oil leaks observed when the turbocharger was removed. On a subsequent visit to the salvage facility by NTSB personnel, the turbocharger’s oil scavenge line was examined and found clear of debris. There were no leaks or residual oil observed on the belly of the airplane.

The turbocharger was disassembled and inspected. The internal components, including the rotor assembly, bearings, and housing, showed no evidence of damage and were covered in a thick coat of oil and debris. No mechanical deficiencies were observed that would have precluded normal operation.

Examination of the engine revealed a large hole in the top of the crankcase between the No. 3 and No. 4 cylinders. The crankshaft was seized and could not be manually rotated. The oil filler cap was secure to the engine. The oil sump was filled with a large amount of metallic debris including a connecting rod and lifters. The oil scavenger pump and the oil pump were removed and rotated manually. Both pumps were disassembled and no mechanical deficiencies were observed.

Disassembly of the engine revealed multiple failed and heavily damaged connecting rods; indications of overheating consistent with oil starvation were found on the Nos. 2 through 5 connecting rods. The Nos. 4 and 5 connecting rods exhibited the most damage and both released from the crankshaft. The camshaft was also sheared and the No. 4 push rods were bent. All of the oil ports were clear except for the No. 5 connecting rod journal, which was blocked, consistent with having been welded over from heat during the failure sequence. The crankshaft would not rotate due to internal damage of the engine; thus, compression and engine timing could not be established.

The airplane was equipped with a Garmin GEA-24 engine indicating system; however, the unit did not have recording capability and no engine data was recovered from the device.

Review of the engine’s maintenance logs indicated that, at the time of the accident, the total operational time of the engine was 2,748 hours. The engine had undergone a major overhaul 871 operational hours before the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA24LA143