N6569GRUMMAN G1642024-08-09 NTSB Accident Report

Substantial
None

GRUMMAN G164S/N: 709

Summary

On August 09, 2024, a Grumman G164 (N6569) was involved in an incident near Dyess, AR. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

On August 9, 2024, about 1600 central daylight time, a Grumman G-164A, N6569, was substantially damaged when it was involved in an accident near Dyess, Arkansas. The pilot was seriously injured. The flight operated under the provisions of Title 14 Code of Federal Regulations Part 137 as an aerial application flight. The pilot stated that when he departed the strip, the engine was performing normally. About ½ mile from the grass strip, the airplane had climbed to 120 ft above ground level, when the pilot could no longer climb or maintain level flight. The pilot maneuvered the airplane below power lines and the airplane’s landing gear contacted a rice field.

This incident is documented in NTSB report CEN24LA313. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N6569.

Accident Details

Date
Friday, August 9, 2024
NTSB Number
CEN24LA313
Location
Dyess, AR
Event ID
20240812194896
Coordinates
35.590623, -90.183227
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The improper overhaul of the carburetor and the malfunction of left magneto which resulted in a partial loss of engine power.

Aircraft Information

Registration
Make
GRUMMAN
Serial Number
709
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
G164G64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
G-164A

Registered Owner (Current)

Name
BENNETT JEANNETTE DBA
Address
2855 W COUNTY ROAD 1020
City
JOINER
State / Zip Code
AR 72350-2601
Country
United States

Analysis

On August 9, 2024, about 1600 central daylight time, a Grumman G-164A, N6569, was substantially damaged when it was involved in an accident near Dyess, Arkansas. The pilot was seriously injured. The flight operated under the provisions of Title 14 Code of Federal Regulations Part 137 as an aerial application flight.

The pilot stated that when he departed the strip, the engine was performing normally. About ½ mile from the grass strip, the airplane had climbed to 120 ft above ground level, when the pilot could no longer climb or maintain level flight. The pilot maneuvered the airplane below power lines and the airplane’s landing gear contacted a rice field. The airplane settled into the rice and abruptly nosed over which resulted in substantial damage to the fuselage and wings.

According to the pilot’s weight and balance calculation, at the time of the accident, the airplane was about 350 pounds under the maximum gross weight. The engine had accumulated 9,652 hours total time in service, and about 1,338 hours since overhaul. The pilot reported that he experienced a similar partial loss of engine power about a week before, but he was able to continue flight by jettisoning the load. No maintenance actions were recorded following this event.

A postaccident examination of the engine at a radial engine repair facility found that carburetor was seized and the left magneto would not produce spark when rotated, but the right magneto did produce spark. The left magneto malfunction to produce spart was not determined. The carburetor was sent to an accessory shop for examination. Disassembly of the carburetor revealed the economizer needle was the incorrect part. In addition, the graphite packing was excessively tight, which affected the needle spring’s ability to properly seat the needle in a downward position. The needle being allowed to remain in an upward position would result in overly rich mixture.

A review of the maintenance logbooks found that the carburetor was overhauled and installed back on the engine on August 22, 2023, at a tachometer time of 1,271 hours. The most recent inspection was a combined annual and 100-hour inspection which was logged on December 10, 2023, and the airplane had flown about 38 hours since those inspections.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN24LA313