N814B

Substantial
Serious

ALEXANDER S ROLINSKI BOT JOURNEYS/N: SC20-014

Accident Details

Date
Wednesday, November 27, 2024
NTSB Number
ERA25LA062
Location
Ocean Isle Beach, NC
Event ID
20241128195559
Coordinates
33.909320, -78.434686
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Aircraft Information

Registration
Make
ALEXANDER S ROLINSKI
Serial Number
SC20-014
Engine Type
4-cycle
Year Built
2021
Model / ICAO
BOT JOURNEYBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
BOT JOURNEY

Registered Owner (Current)

Name
SANTOS RICHARD A
Address
416 SEABURY LN
City
MYRTLE BEACH
State / Zip Code
SC 29579-3813
Country
United States

Analysis

On November 27, 2024, about 1319 eastern standard time, an experimental amateur-built Bot Journey airplane, N814B, was substantially damaged when it was involved in an accident near Ocean Isle Beach, Norh Carolina. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 test flight.

The test flight occurred at Odell Williamson Municipal Airport (60J), Ocean Isle Beach, North Carolina.

According to the pilot, who was also a light sport aircraft repairman, the airplane was recently equipped with a Rotax 912ULS engine, which was “running poorly.” A few days prior to the accident, the airplane experienced a total loss of engine power while a flight instructor was conducting ground runs, which included takeoff accelerations on the runway. Upon troubleshooting, the pilot discovered that the floats on both carburetors were damaged and installed improperly. He then installed new floats in accordance with the Rotax Maintenance Manual. He also replaced all 8 spark plugs with new spark plugs and performed maintenance to the cowling and inspected the brakes. The pilot and flight instructor subsequently performed several ground runs of the airplane’s engine over a 2-day period.

On the day of the accident, the pilot continued operating the airplane on the ground, which included performing high speed taxi checks. All systems were normal and the engine idle was smooth. The pilot then intended to conduct a functional test flight in the 60J traffic pattern before releasing the airplane for use in pilot training.

The pilot taxied the airplane to runway 06, applied full throttle and checked that all systems were indicating in the green, and that the engine rpm was at approximately 5,100. The takeoff was normal with all systems in the green. Upon reaching 200 ft msl, the engine abruptly stopped without any warning or fluctuation in rpm. The propeller was “fixed” (not moving). The pilot performed an immediate left turn to attempt to stay over the airport and pitched forward to maintain a glide speed of 40 mph; however, it became clear that the airplane was going impact trees. As the airplane neared the treetops, the pilot pulled hard aft on the control stick to stall the airplane and minimize forward speed and impact forces.

The pilot did not remember the impact. He egressed from the airplane and subsequently crawled to the edge of the woods where two individuals discovered him. First responders arrived shortly thereafter.

The wreckage was retained by the NTSB for examination.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA25LA062