N403LC

Substantial
None

LOCKHEED 382G-44K-30S/N: 4590

Accident Details

Date
Thursday, December 19, 2024
NTSB Number
DCA25LA061
Location
St. Mary's, AK
Event ID
20241220199449
Coordinates
62.097638, -162.600600
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Aircraft Information

Registration
Make
LOCKHEED
Serial Number
4590
Engine Type
Turbo-prop
Year Built
1975
Model / ICAO
382G-44K-30
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
4
Seats
3
FAA Model
382G-44K-30

Registered Owner (Current)

Name
LYNDEN AIR CARGO LLC
Address
6441 S AIRPARK PL
City
ANCHORAGE
State / Zip Code
AK 99502-1809
Country
United States

Analysis

On December 18, 2024, about 1600 Alaska standard time (AKST), Lynden Air Cargo LLC flight LYC141, a Lockheed L-382C (Hercules) airplane, N403LC, experienced a rapid decompression while climbing through FL220 (22,000 ft) after departure from the St. Mary’s airport (KSM), St. Mary’s, Alaska. There were no injuries to the four occupants onboard the airplane. A postaccident inspection revealed that the airplane sustained substantial damage. The regularly scheduled cargo flight was operating under the provisions of Title 14 Code of Federal Regulations Part 121 from KSM to the Ted Stevens Anchorage International Airport (ANC), Anchorage, Alaska.

History of Flight

The flight crew consisted of the captain who was the pilot monitoring, the first officer (FO) who was the pilot flying and the flight engineer. In addition, a load master was present on the flight. The flight crew reported that after departure from KSM and while climbing through about FL220 they heard a loud bang followed by a loss of pressurization. They donned their oxygen masks and initiated a descent to 13,000 ft mean sea level (msl).

With no visible sign of damage, the flight crew suspected a bleed air problem. The quick reference handbook (QRH) was reviewed and all bleed air systems turned off. The flight crew elected to continue to their destination. About 30 minutes before arrival to ANC, the number 3 engine’s torque began to fluctuate. Concerned that the torque fluctuations were related to the bleed air systems they decided on a precautionary shutdown of the number three engine in accordance with the QRH and Lynden Air Cargo’s procedures. An emergency was declared with air traffic control and the flight continued to ANC and landed without further incident.

A post flight inspection by maintenance personnel revealed a crack in the forward pressure bulkhead, see figure 1. The fracture was harvested by maintenance personnel and shipped to the NTSB Materials Laboratory for further examination.

Figure 1. Location of the crack found in forward pressure bulkhead is shown within the red circle. (Source: Lynden Air Cargo LLC)

As part of the investigative process, the NTSB invited the qualified parties to participate in the investigation. These included the Federal Aviation Administration (FAA), and Lynden Air Cargo LLC.

The parties were formed into specialized investigative groups led by NTSB group chairs in the areas of structures and digital flight data recorder (DVDR).

The investigation continues.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DCA25LA061