N77LH

Destroyed
None

LANCAIR 360S/N: 891 320 688

Accident Details

Date
Thursday, June 12, 2025
NTSB Number
CEN25LA205
Location
Fort Stockton, TX
Event ID
20250612200314
Coordinates
30.915259, -102.916450
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Aircraft Information

Registration
Make
LANCAIR
Serial Number
891 320 688
Engine Type
Reciprocating
Year Built
1999
Model / ICAO
360
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
LOVEAIR 360

Registered Owner (Current)

Name
REGISTRATION PENDING
Address
2606 SE 21ST AVE
City
CAPE CORAL
State / Zip Code
FL 33904-3268
Country
United States

Analysis

On June 11, 2025, about 2145 central daylight time, a Lancair 360 airplane, N77LH, was destroyed when it was involved in an accident near Fort Stockton, Texas. The airline transport pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, he had recently purchased the airplane in California, and he was performing a cross-country flight to his home base in Florida. The airplane stopped at the El Paso International Airport (ELP), El Paso, Texas to refuel. The airplane departed from ELP about 1940 mountain daylight time. While enroute to the San Antonio International Airport, San Antonio, Texas, the pilot smelled smoke in the cockpit. The pilot contacted air traffic control and changed his destination airport to the Fort Stockton-Pecos County Airport, Fort Stockton, Texas, due to the emergency. Once the pilot maneuvered the airplane for landing on runway 12, the cockpit was filled with smoke, and flames were emitting from underneath the instrument panel.

During the landing, the pilot reported he did not have brake authority, and the airplane departed the runway to the left. The airplane came to rest upright against a barbed wire fence along the airport perimeter. The pilot was able to egress from the airplane without further incident.

The fire consumed the engine compartment, part of the fuselage, and the left wing. The wreckage was recovered from the accident site, and it was transported to a secure location for future examination.

The experimental airplane was built from a kit in 1999. The composite construction airplane was equipped with a Lycoming Engines O-360-A1A reciprocating engine. The airplane had a condition inspection performed by a mechanic on the airframe and the engine on June 9, 2025. During the inspection, it was noted that the airframe had accumulated 440.4 hours total time, and the engine had accumulated 2,220.9 hours total time (with 911.9 hours since overhaul). The pilot reported that the airplane maintenance records and the historical airplane build records were stored in the baggage compartment and consumed by the fire.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN25LA205