Summary
On June 09, 2025, a Mooney M20R (N9166Z) was involved in an incident near New Port Richey, FL. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
On June 9, 2025, about 0600 eastern daylight time, a Mooney, M20R airplane, N9166Z, was substantially damaged when it was involved in an accident near New Port Richey, Florida. The commercial pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that he departed Inverness Airport (INF), Inverness, Florida and flew for about 15 minutes to Hidden Lake Airport (FA40), New Port Richey, Florida where he intended to land. During the landing flare to runway 5, a 4,425-ft-long runway, the airplane floated; the pilot reported that he was uncomfortable trying to land on the remaining runway, so he executed a go-around, by adding full power and setting the flaps for climb. During the maneuver, at about 50 ft.
This incident is documented in NTSB report ERA25LA273. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N9166Z.
Accident Details
Probable Cause and Findings
The pilot's mismanagement of the available fuel, which resulted in fuel starvation and a total loss of engine power.
Aircraft Information
Registered Owner (Current)
Analysis
On June 9, 2025, about 0600 eastern daylight time, a Mooney M20R airplane, N9166Z, was substantially damaged when it was involved in an accident near New Port Richey, Florida. The commercial pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
About 40 days after the accident occurred, the pilot reported that he departed Inverness Airport (INF), Inverness, Florida, and flew for about 15 minutes to Hidden Lake Airport (FA40), New Port Richey, Florida, where he intended to land. During the landing flare to runway 5, which was 4,425 ft long, the airplane floated; the pilot reported that he was uncomfortable trying to land on the remaining runway, so he executed a go-around by adding full power and setting the flaps for a climb. During the maneuver, about 50 ft above the runway, the engine stopped producing power. There was no hesitation or “engine cough” that preceded the loss of power, and the pilot did not observe low fuel warning lights. The airplane was too low for the pilot to fully troubleshoot, so he switched fuel tanks, but that did not restore power and the airplane began to descend.
The airplane descended into the runway overrun area and impacted brush and muddy terrain before coming to rest upright. Postaccident examination confirmed substantial damage to the wings and fuselage. The right wing sustained damage to the wing spar, and there were multiple buckles and dents throughout the fuselage.
According to the pilot, he should have had at least 17 gallons remaining in the fuel tanks at the time of the accident, based on his estimation of the airplane’s fuel consumption and the most recent fueling on June 1, 2025.
A subsequent examination and engine test run was performed. The fuel-injected engine was operated with no anomalies observed. Fuel was subsequently drained from the fuel tanks. No contamination or water was observed in the fuel. The total amount of fuel drained from the left wing tank was about 2.5 gallons. The right wing tank contained about 13 gallons of fuel. The unusable amount of fuel per side was 3 gallons according to the Airplane Operating Manual.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA25LA273