N6191M

Substantial
None

Stinson 108-3 S/N: 108-4191

Accident Details

Date
Sunday, February 21, 1999
NTSB Number
NYC99LA065
Location
BRISTOL, CT
Event ID
20001205X00235
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The partial loss of power due to the failure of a fatigued connecting rod bolt.

Aircraft Information

Registration
N6191M
Make
STINSON
Serial Number
108-4191
Engine Type
Reciprocating
Year Built
1948
Model / ICAO
108-3 S108
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
N C CUTHBERT LLC
Address
54 NORRIS ROAD
Status
Deregistered
City
DENVILLE
State / Zip Code
NJ 07834
Country
United States

Analysis

On February 21, 1999, about 1158 Eastern Standard Time, a Stinson 108-3, N6191M, was substantially damaged when it impacted the ground during a forced landing near Bristol, Connecticut. The certificated private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight conducted under 14 CFR Part 91.

The pilot stated he had just terminated communications and radar services from the Bradley Windsor Locks TRACON, when he heard a loud noise accompanied by a loss of power. The pilot began a left-hand turn to search for a place to land. The pilot then transmitted to the radar controller that he was declaring an emergency and landing the airplane into a field. The field had an approximate length of 1,000 feet. As the airplane approached the field heading north, the pilot shut the engine down and was unable to slow the airspeed enough to make a landing at the beginning of the field. Approximately 400 feet from a tree line at the end of the field, the main wheels touched down and the pilot applied braking. Due to the excessive speed the airplane was light on it's wheels and the brakes were ineffective. The pilot attempted to turn to the left to avoid the tree line, but struck three small trees. The airplane came to rest in an upright position facing east.

An inspection of the engine by the Federal Aviation Administration revealed two holes in the top of the engine crankcase. The engine was retained, and examined on March 12, 1999. The number 3 and 4 cylinders were damaged extensively, and removed from the crankcase. The Number 3 piston and connecting rod were found separated from the crankshaft. The connecting rod bolts were found in the oil sump pan. The number four piston and connecting rod remained connected to the crankshaft, and exhibited metal pinging on the piston skirt and rod. The connecting rod bolts were attached to the rod.

The number 3 piston, and it's connecting rod and bolts, were forwarded to the National Transportation Safety Board Materials Laboratory, Washington, DC, for examination. According to the Metallurgist's Factual Report, one of the connecting rod bolts contained microfissures typical of fatigue cracking on the head portion of the bolt. The fatigue cracking initiated from multiple locations on one side of the underhead radius, and had propagated nearly all of the way through the cross section of the bolt before final separation.

A review of the Airplane Engine logbooks revealed that the last Major overhaul was conducted on March 3, 1965, with a recorded total time of 1,612 hours. The pilot reported a total airframe time of 2,593 hours at the time of the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC99LA065