N22710

Substantial
None

Cessna 150H S/N: 15068464

Accident Details

Date
Sunday, April 18, 1999
NTSB Number
LAX99LA155
Location
YUBA CITY, CA
Event ID
20001205X00502
Coordinates
39.050163, -121.609695
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power resulting from the fatigue failure of a cylinder's exhaust valve. A contributing factor was the uneven terrain at the forced landing site. The reason for the fatigue could not be determined.

Aircraft Information

Registration
N22710
Make
CESSNA
Serial Number
15068464
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
150H C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
19747 HIGHWAY 59 N STE 314
Status
Deregistered
City
HUMBLE
State / Zip Code
TX 77338-3504
Country
United States

Analysis

On April 18, 1999, at 0914 hours Pacific daylight time, a Cessna 150H, N22710, owned and operated by the pilot, experienced a loss of engine power en route to Shelter Cove, California. The pilot made a forced landing in a wheat field near Yuba City, California. During rollout, the airplane encountered uneven terrain, nosed over, and was substantially damaged. The airline transport certificated pilot was not injured. Visual meteorological conditions prevailed during the personal flight, and a visual flight rules flight plan was filed. The flight was performed under 14 CFR Part 91, and originated from the uncontrolled Sutter County Airport in Yuba City, at 0856.

The pilot indicated to the National Transportation Safety Board investigator that he was familiar with the operation of his airplane. He holds a certified flight instructor certificate and reported having over 10,275 hours of flight time.

According to the pilot, following a normal takeoff he climbed to 2,000 feet mean sea level and began cruising toward his destination. After a few minutes, he felt a "bump," and the engine began losing power. However, no unusual vibrations were detected. The pilot stated that despite his application of carburetor heat and adjustment of the mixture control, the engine progressively lost all power until the propeller was eventually just windmilling.

In the pilot's completed report, he indicated that his airplane's total time was 8,798.6 hours. The engine had been operated for 1,818.9 hours since being overhauled, and 133.4 hours since its last inspection.

The Federal Aviation Administration coordinator verbally reported to the Safety Board investigator that an examination of the engine revealed its No. 2 cylinder exhaust valve was fatigued and broken. No other engine related malfunctions were observed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA155