N9614U

Substantial
None

GRUMMAN AA-1A S/N: AAIC-OO72

Accident Details

Date
Saturday, February 12, 1994
NTSB Number
LAX94LA121
Location
BISHOP, CA
Event ID
20001206X00767
Coordinates
37.499870, -118.310928
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

fuel exhaustion due to the pilot's inadequate preflight planning and en route fuel consumption monitoring.

Aircraft Information

Registration
N9614U
Make
GRUMMAN
Serial Number
AAIC-OO72
Engine Type
Turbo-shaft
Year Built
1977
Model / ICAO
AA-1A V1
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SALE REPORTED
Address
19149 CR NS238
Status
Deregistered
City
GRANDFIELD
State / Zip Code
OK 73546
Country
United States

Analysis

On February 11, 1994, at 1740 Pacific standard time, a Grumman AA-1A, N9614U, lost engine power while in cruise and nosed over in soft soil near Bishop, California, during a forced landing in a field. The aircraft was owned and operated by the pilot. Visual meteorological conditions prevailed at the time and no flight plan was filed for the operation. The aircraft incurred substantial damage. The certificated private pilot and his one passenger were not injured. The flight originated at Santa Monica, California, on the day of the mishap at 1455 as a cross- country personal flight to Mammoth Lakes, California.

In his written report, the pilot stated that he departed with full fuel, and on the left fuel tank. At 1610 hours, the pilot switched to the right fuel tank when the gauge for the left indicated approximately one-quarter. The pilot overflew Bishop at about 1720 hours climbing from an en route cruise altitude of 7,500 feet to 9,500 feet for mountainous terrain. Shortly thereafter, the pilot switched back to the left fuel tank and the engine quit. The pilot said he immediately turned on the electric boost pump and switched back to the right tank; the engine ran for a few minutes, then quit again. The pilot was unable to obtain an engine restart thereafter.

The pilot reported that at the time the engine problem began, he turned around and headed for the Bishop airport, which was at an estimated distance of 12 miles. The aircraft had insufficient altitude to reach the airport and the pilot landed in a field. The aircraft encountered soft soil and nosed over.

The aircraft retrieval firm which recovered the aircraft reported that no fuel was found in the aircraft tanks. The soil beneath the aircraft was examined, with no odor of fuel evident.

After recovery of the aircraft, the fuel system was examined by a mechanic at the wreckage storage facility. Both the engine driven and electric boost pumps were found to function normally. No obstructions were noted in either the fuel selector or system lines. No fuel was found in the fuel lines from the wing root to the fuel selector, and only residual fuel was noted in the fuel line from the selector valve to the electric boost pump.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX94LA121