N2495L

Destroyed
Fatal

PIPER PA-38-112 S/N: 38-79A0734

Accident Details

Date
Saturday, March 5, 1994
NTSB Number
CHI94FA097
Location
INMAN, KS
Event ID
20001206X00857
Coordinates
38.220001, -97.770355
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

AN UNINTENTIONAL SPIN WHICH OCCURRED DURING THE MANEUVERING PHASE OF A BIENNIAL FLIGHT REVIEW. A FACTOR RELATED TO THE ACCIDENT WAS: THE AIRPLANE'S LATERAL-DIRECTIONAL CHARACTERISTICS AT OR NEAR THE STALL SPEED.

Aircraft Information

Registration
N2495L
Make
PIPER
Serial Number
38-79A0734
Engine Type
Reciprocating
Model / ICAO
PA-38-112 PA38
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HALL MARVIN L DBA
Address
HUTCHINSON MUNICIPAL AIRPORT 126
Status
Deregistered
City
HUTCHINSON
State / Zip Code
KS 67501
Country
United States

Analysis

HISTORY OF FLIGHT

On March 5, 1994, at 0830 central standard time (cst), a Piper PA-38-112, N2495L, registered to Marvin Hall dBa Hutchinson Aviation, of Hutchinson, Kansas, with a commercially certificated flight instructor administering a biennial flight review (flight review) to a private pilot, was destroyed during a collision with the ground and subsequent fire. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 flight was not operating on a flight plan. Both pilots were fatally injured. The flight departed Hutchinson, Kansas, at 0800 cst.

Three witnesses said they observed the airplane during its descent to the ground. Two witnesses observed the airplane in a five or six turn spin to the left. One witness said he saw the spin stop just above the ground, with the airplane's "...nose pulled up slightly, but then back down before it hit."

During the interview the witnesses were asked to show, with a model airplane, what N2495L had been doing during its descent to the ground. Each witness made a motion with the model airplane that replicated a left spin that had an approximate 45 degree nose down attitude.

PERSONNEL INFORMATION

The logbook for the pilot receiving the flight review was destroyed in the post crash fire. According to Federal Aviation Administration (FAA), the pilot obtained his private pilot certificate on November 27, 1991. The pilot reported he had 50 hours of flight time when he obtained his second class medical certificate on March 20, 1992. The pilot's supervisor said that to his knowledge the pilot was current and had taken annual leave to obtain a biennial flight review before his currency expired.

The flight review recipient's wife stated he had accumulated about 75 to 100 hours of flying time since obtaining his private pilot certificate. She said her husband had told her that his flight check was due before they moved to Des Moines, Iowa, in May 1994. The wife of the flight instructor administering the flight review stated the other pilot had not flown the PA-38 since May 21, 1993, according to company records.

The flight instructor administering the flight review had completed an FAA airman competency flight check according to 14 CFR Part 135.293, .297, and .299 on December 31, 1993. This pilot's number three logbook showed he had a total time of 7,944.9 hours, 1,803.5 hours as a flight instructor, as of January 25, 1994. The logbook began with the entry of August 16, 1985, showing a total flight time of 4,943.2 hours. The first Piper PA-38 (PA-38) logbook entry was made on August 18, 1985. The pilot's total flying time in the PA-38, as found in the number three logbook, was 104.9 hours. Complete pilot logbook records were not made available for review. The NTSB Form 6120.1/2 that was sent to the pilot's wife was not returned. She did say that he had a total time of 745 hours in the Piper PA-38.

The instructor's flight review methodology was revealed during interviews with two pilots and a written statement from a third pilot. One pilot said the instructor had him do approach to landing, and takeoff and departure stalls on headings and in turns. He said that he demonstrated these stalls to the instructor with landing flaps retracted and extended. The second pilot said the instructor asked to see imminent stalls only. His written statement said, "...I proceeded one time to go to a full stall and Marvin quickly detoured that route."

A pilot, training for a flight instructor rating, said the instructor had spun the PA-38 on several occasions during his training. He said the instructor had demonstrated one turn spins to him and that he had performed spins under his direction. The pilot said the instructor had discussed stalls, spin entry, and spin recovery with him during ground training. He said the instructor had told him to avoid getting the airplane into a spiral and that he had to enter the spin forcefully.

AIRCRAFT INFORMATION

The PA-38 was certified under the Delegated Option Authority granted to manufacturers of aircraft by the FAA. The PA-38 received its airworthiness certificate from the FAA on December 20, 1977. The PA-38 was certified in the utility and normal category by the FAA. This certification allowed it to perform spins when operated in the utility category.

According to the pilots operating handbook (POH), "Normal recoveries may take up to 1 1/2 turns when proper technique is used; improper technique can increase the turns to recover and the resulting altitude loss." The POH continues, "In all spin recoveries the control column should be moved forward briskly, continuing to the full forward stop if necessary. This is vitally important because the steep spin attitude may inhibit pilots from moving the control column forward positively."

The POH says "...one half of the spin [rotation takes]... about one second... . Improper application of recovery controls can increase the number of turns to recover and the resulting altitude loss. Delay of more than about 1-1/2 turns before moving the control wheel forward may result in the aircraft suddenly entering a very fast, steep spin mode which could disorient a pilot. Recovery will be achieved by briskly moving the control wheel fully forward and holding it there while maintaining full recovery rudder." "If such a spin mode is encountered, the increased rate of rotation may result in the recovery taking more turns than usual after the control column has been moved fully forward. A one-turn spin, properly executed, will require 1,000 to 1,500 feet to complete and a six-turn spin will require 2,500 to 3,000 feet to complete."

Three Piper Aircraft Corporation Service Bulletins (Numbers 609, 661 and 800) were issued on the PA-38's control column. Number 609 dealt with ensuring that the control column (tube) was securely welded to the control wheel. This service bulletin was made into a Federal Aviation Administration Airworthiness Directive (AD). Service bulletin numbers 661 and 800 dealt with the binding of the control column when positioned fully aft (full up elevator).

According to N2495L's airframe logbooks, service bulletins 661 and 800 were complied with. Service Bulletin 609, and its accompanying airworthiness directive, did not apply to N2495L.

WRECKAGE AND IMPACT INFORMATION

N2495L collided with the ground on an approximate magnetic heading of 040 degrees. The first ground scar was oriented on an approximate magnetic heading of 130/310 degrees, measuring about 38 feet. A second ground scar, originating from the midpoint of the first, was about 120 feet long and on a magnetic heading of 345 degrees. The second ground scar led to N2495L's wreckage. The airplane's wreckage heading was 355 degrees magnetic.

The first ground scar varied in depth between two and four inches. It had white paint transferred onto sections of compressed dirt. A piece of curved, green, glass was found at the extreme southeast edge of this ground scar. At the center of this ground scar an elliptically shaped depression measuring about five feet wide and six feet long. It was about seven inches deep at the center. Gouge marks were found in the approximate center of this area. The largest gouge mark matched one of the airplane's propeller blades. Examination of the blade found chordwise scratches, some having the same colored dirt in them as found in the gouge.

The main landing gear legs had separated from the fuselage mounts. One main landing gear was found on top of the left wing at the mid-span position. A second main landing gear leg was found about 100 feet northwest of the first ground scar termination point. The wheel and tire assemblyies were attached to the main landing gear legs. The tires matched ground indentations that were found south of the elliptically shaped ground depression. The ground indentations were equally spaced on either side of the elliptically shaped ground depression.

The inboard sections of the both wings were burnt. The fuselage had burned between the engine compartment and vertical stabilizer. The propeller had partially separated from the crankshaft flange. The propeller was 'S' shaped, one blade curved forward about 90 degrees from its hub. The second blade was curved aft about 40 degrees from its mid-span position.

The right wing was twisted about 70 degrees upward at the mid-span point outward to its wingtip. Leading edge skin on the wing was wrinkled and had separated from the main wing spar. The inboard portion of the leading edge skin was burnt. The ground under the right wing fuel tank area had a strong odor of aviation gasoline. The left wing leading edge skin was wrinkled.

Flight control continuity between the respective surfaces and control yokes and rudder pedals was confirmed. The left control yoke/mounting sleeve combination had separated from its torque tube. The right control yoke was attached to its torque tube. The control yoke torque tubes, chain sprockets, chains, and tee bar assembly was found complete and unseparated.

The elevator and rudder stops were not damaged. Elevator trim cable and springs were fire damaged. They were attached between the cockpit trim wheel and trim tab. The top of the left rudder stop was 3/8" from the vertical stabilizer spar mount. The top of the right rudder stop was 5/16" from the vertical stabilizer spar mount.

The engine was fire damaged; it was rotated confirming internal component continuity when the magnetos were removed. The right magneto was fire and impact damaged and could not be turned. The left magneto was fire damaged but could be rotated. The carburetor had separated from its mounting flange and was fire damaged. The muffler had been crushed aft and upward into the engine's sump.

ADDITIONAL INFORMATION

Research into the PA-38's design, certification, and manufacture revealed the d...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI94FA097