N890US

MINR
None

FOKKER F28 MK 0100 S/N: 11365

Accident Details

Date
Sunday, May 1, 1994
NTSB Number
ATL94IA088
Location
CHARLOTTE, NC
Event ID
20001206X01204
Coordinates
35.230014, -80.910400
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
94
Total Aboard
94

Probable Cause and Findings

THE IMPROPER RIGGING OF THE NOSE WHEEL STEERING SYSTEM BY COMPANY MAINTENANCE PERSONNEL.

Aircraft Information

Registration
N890US
Make
FOKKER
Serial Number
11365
Engine Type
Turbo-jet
Year Built
1991
Model / ICAO
F28 MK 0100 F100
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
WELLS FARGO BANK NORTHWEST NA TRUSTEE
Address
299 SOUTH MAIN STREET 12TH FL
MAC U1228-120
Status
Deregistered
City
SALT LAKE CITY
State / Zip Code
UT 84111
Country
United States

Analysis

HISTORY OF FLIGHT

On May 1, 1994, AT 1309 eastern daylight time, a Fokker F28 MK 100, N890US, landed without the nose landing gear extended at the Douglas International Airport, in Charlotte, North Carolina. Flight 323 was operated under the provisions of 14 CFR Part 121 by USAir, Inc., as a scheduled, domestic, passenger flight. The airline transport pilot and first officer, three flight attendants, and 89 passengers were not injured. There was minor damage to the airplane. Visual meteorological conditions existed at the time, and an instrument flight rules flight plan was filed for the flight to Charlotte. The flight originated in Detroit, Michigan at 1119.

The flight crew reported the following: This was the third day of the three-day trip sequence, and the first day in this particular aircraft (N890US). On the day of the incident, the only flights flown by them were a flight to Detroit, and the flight to Charlotte (the incident flight). They reported no minimum equipment list entries regarding the landing gear system. There was an entry from the previous flight crew which stated that the nose wheel steering would occasionally bind while in operation. The nose wheel steering performed normally during the flight to Detroit, and the flight crew was not aware of any maintenance being performed on the aircraft in Detroit. The ground, takeoff, and enroute portions of the incident flight were normal. Approaching Charlotte, the flight was cleared for a visual approach to runway 18R. At 2,000 to 1,700 feet above ground level (agl), the landing gear handle was lowered. At approximately 1,300 feet agl, the main gear "snapped" into position. The nose gear indicated an "in transit" condition. They performed a missed approach, climbed to a higher altitude, and set the autopilot on. They attempted to recycle the gear, and again observed the "in transit" light on the nose gear, with the nose gear indicating that it was not down and locked. The first officer read the checklist, as the captain flew the airplane. The alternate landing gear extension checklist was performed, and the nose gear still did not indicate down and locked. The partial gear checklist was read, and Air Traffic Control personnel informed them that the nose gear appeared to be up. The aircraft was landed on runway 18R, and an emergency evacuation was accomplished. The captain reported that the antiskid switch was on when the aircraft was landed.

PERSONNEL INFORMATION

Information on the captain is included in this report at the section titled "First Pilot Information." Information on the first officer is included in Supplement E, attached to this report.

AIRCRAFT INFORMATION

The nose wheel steering (NWS) system on this aircraft consists of the following main components (shown in figures 1, 2, and 3, attached to this report):

- The steering handwheel (tiller), which is connected to the rudder interface unit (IFU) through cables. - The rudder pedals, which are connected to the rudder IFU through a lever on the rudder torque tube and a push-pull rod. - The rudder IFU, which controls the NWS control unit through cables. - The NWS control unit, which operates the steering control valve when there is a difference between the selected and actual steering angles. - A nose wheel steering shut off valve which, when closed by the energized solenoid, prevents hydraulic pressure and flow to the steering control valve, and thus prevents the nose gear turning tube from turning. - The steering control valve, which controls the steering motor, which in turn operates the nose landing gear (NLG) turning tube with the sliding member and nose wheels. - A position feedback cable, which controls the steering control valve via the nose wheel steering control unit, such that the steering motor stops operating when the nose wheels are in the selected position. - A centering mechanism, to center the NLG when the landing gear lever has been selected to the up position.

An input in the NWS system can be given by the tiller (up to 76 degrees either side). The steering input is supplied via the IFU to the NWS control unit. The tiller can override rudder pedal steering commands.

On the NWS control unit are the pulleys for the input cables (from the rudder IFU) and the position feedback cables (from the NLG turning tube). The pulley system controls the steering control valve through an idler bar. When there is a steering input, the idler bar starts to turn. When the idler bar moves, it gives an input to the steering control valve, which allows hydraulic pressure to the NLG steering motor. When the NLG starts to turn, the position feedback cables move pulleys A and B (which are connected to each other). As a result, the idler bar turns back to the neutral position. The steering control valve is back in the neutral position when the nose wheels are in the selected position.

The centering mechanism centers the NLG after a gear up selection, through the use of a centering cam and cam rollers (see figure 3). When the NLG moves during steering, the feedback input moves the cam. From the moment the landing gear lever is selected to the up position (pressure in the up lines), the centering actuator is pressurized, and extends, pushing the cam against the cam follower, through rollers. When the nose wheels are not in the centered position, the cam and follower are not aligned, and the cam contacts the rollers as the centering actuator is extended. This gives an input to the steering control valve. Because the NWS system is still pressurized, the NLG moves to the centered position during retraction. Hydraulic pressure in the up lines maintains the NLG in the retracted and centered position during flight. From the moment the landing gear lever is selected to the down position, (1) an electrical circuit energizes the nose wheel steering shut off valve solenoid, and thus depressurizes the NWS system, and (2) the hydraulic up lines and thus the centering actuator are depressurized, and the centering actuator is retracted by spring force. This causes the cam to disengage from the cam follower, and deactivates the centering mechanism. Via ground flight switches and a time delay relay, the nose wheel steering shut off valve solenoid remains energized, and thus the nose wheel steering system remains depressurized, until five seconds after touchdown.

The aircraft maintenance records revealed that on April 14, 1994, a leaking nosewheel steering control valve was found. The steering control valve was replaced on April 20, 1994, during scheduled maintenance. According to the Fokker 100 Aircraft Maintenance manual (Procedure 32-52-02, Steering Control Valve Removal/Installation), an operational test of the steering control valve (after replacement) includes two checks if the nose wheels return to the center position: the first after the hydraulic system is pressurized, and the second after the steering handwheel and thus the NLG has been turned left and right.

An inspection of the aircraft maintenance records revealed that an incorrect procedure number was entered after the steering control valve was replaced. Procedure number 32-52-01 (Steering Shut-off Valve Removal and Installation) was entered instead of procedure number 32-52-02. The mechanic who performed the work reported that although procedure number 32-52-01 was entered in the records, he used procedure number 32-52-02, the correct procedure. It was noted that procedure number 32-52-01 calls for a visual inspection of the nose wheel operation to the center position, and does not require the use of the rigging indicator tool, as does procedure number 32-52-02.

Two flights prior to the incident flight, the flight crew entered into the aircraft maintenance logbook that the nosewheel steering would occasionally bind, when turning. The corrective maintenance action was to lubricate the nose landing gear. During the post-incident investigation, it could not be determined which parts of the nose landing gear had been lubricated.

METEOROLOGICAL INFORMATION

Weather information for Charlotte, North Carolina (CLT) is included in this report at the section titled "Weather Information."

WRECKAGE AND IMPACT INFORMATION

The aircraft came to rest on runway 18R, with its nose on the runway, and the nose gear inside the wheel well. An examination of the runway revealed four parallel black skid marks, each about 115 feet in length, leading to the main gear tires. The main gear tires exhibited flat spots, consistent with skidding. The antiskid switch was found in the "on" position during the documentation of the cockpit.

An inspection of the runway surface revealed a 12 inch long, quarter inch drive ratchet extension in the middle of the runway, about 100 feet north of the main tire skid marks. No witness marks were found on the extension, other than light scraping signatures, consistent with runway surface scraping. An examination of the NLG wheel well did not reveal positive evidence of the tool having been wedged in the well. The origin of the extension was not determined.

During the investigation, a kink was found in the lower feedback cable of the nose wheel steering system. The function of the cable is described in the "Aircraft Information" section of this narrative. The origin of the kink was not positively determined.

The aircraft lower, forward fuselage, (NLG) wheel well, and NLG doors were damaged from scraping contact with the runway surface. Portions of the NLG doors and door hold-open rods were found inside the wheel well. The left NLG door casting (at the end of the hold-open rod) exhibited runway scraping at two different angles. One angle was consistent with the door full open position, and the other was indicative of a partially opened position.

The nose of the aircraft was lifted from the runway surface with air bags. As the nose was raised from the runway, the NLG emerged freely from ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL94IA088