Summary
On May 16, 1994, a Stinson 108-2 (N9761K) was involved in an incident near Kettle River, MN. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: THE PILOT'S IMPROPER USE OF CARBURETOR HEAT AND THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING. THE CARBURETOR ICING WEATHER CONDITION WAS A FACTOR.
On May 15, 1994, about 2000 central daylight time, a Stinson 108- 2, N9761K, experienced a loss of engine power during takeoff from a private airstrip near Kettle River, Minnesota. The airplane sustained substantial damage when it struck some trees in the forced landing. The private pilot was not injured. No flight plan was filed for the personal flight, and visual meteorological conditions prevailed at the time.
The pilot stated the engine rpm dropped about 10-12 seconds after lift off, then the engine started sputtering and stopped. Federal Aviation Administration Inspectors who examined the wreckage reported the carburetor and intake manifold were damaged by ground impact. They were not able to determine if the fuel contained any contaminates.
This incident is documented in NTSB report CHI94LA163. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N9761K.
Accident Details
Probable Cause and Findings
THE PILOT'S IMPROPER USE OF CARBURETOR HEAT AND THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING. THE CARBURETOR ICING WEATHER CONDITION WAS A FACTOR.
Aircraft Information
Registered Owner (Current)
Analysis
On May 15, 1994, about 2000 central daylight time, a Stinson 108- 2, N9761K, experienced a loss of engine power during takeoff from a private airstrip near Kettle River, Minnesota. The airplane sustained substantial damage when it struck some trees in the forced landing. The private pilot was not injured. No flight plan was filed for the personal flight, and visual meteorological conditions prevailed at the time.
The pilot stated the engine rpm dropped about 10-12 seconds after lift off, then the engine started sputtering and stopped. Federal Aviation Administration Inspectors who examined the wreckage reported the carburetor and intake manifold were damaged by ground impact. They were not able to determine if the fuel contained any contaminates. The Inspectors stated they were not able to find any engine malfunctions. The temperature was 51 degrees F., and the dew point was 43 degrees F. The pilot stated he checked the operation of the carburetor heat during his pre- takeoff engine run-up. The FAA inspector who examined the wreckage reported the carburetor heat was in the OFF position.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI94LA163