N3736V

Substantial
Minor

CESSNA 140 S/N: 15013

Accident Details

Date
Sunday, August 14, 1994
NTSB Number
SEA94LA211
Location
DAYTON, WY
Event ID
20001206X02141
Coordinates
44.870521, -107.250244
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL.

Aircraft Information

Registration
N3736V
Make
CESSNA
Serial Number
15013
Engine Type
Reciprocating
Year Built
1949
Model / ICAO
140 C140
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
DUFF J W DBA
Address
8131 E 40TH AVE
Status
Deregistered
City
DENVER
State / Zip Code
CO 80207-1712
Country
United States

Analysis

On August 13, 1994, approximately 2000 hours mountain daylight time (MDT), a Cessna 140, N3736V, registered to Sundance Aviation, Inc., and being flown by Dan T. Miller, a private pilot, sustained substantial damage when the right main landing gear collapsed and separated from the aircraft during landing roll at a private airstrip near Dayton, Wyoming. The pilot and passenger received minor injuries. Visual meteorological conditions existed and no flight plan had been filed. The flight, which was personal in nature, was to have been operated in accordance with 14CFR91, and originated from the accident site airstrip approximately 1930 hours.

The pilot reported that the landing was a normal three point touch down. During the roll out, as the airplane slowed and control effectiveness decreased, the aircraft began to gradually veer left. The pilot applied right rudder control, however, the airplane continued to the left. The pilot increased the rudder control and applied braking action, however, the airplane continued to gradually rotate to the left. At the beginning of the left turn, the pilot stated that the airplane sank slightly to the right. The airplane continued to rotate to the left until the left wheel lifted off the ground and the airplane ground looped approximately 135 degrees counter clockwise before coming to a stop.

After the accident, the pilot noted that the right main landing gear separated from the fuselage at its attach point, and was laying approximately ten feet from where the airplane came to rest.

A Federal Aviation Administration Inspector from the Denver, Colorado, Flight Standards District Office inspected the attachment bolt for the right main landing gear and found evidence of an overload separation. The brakes were free from binding and did not reveal evidence of overheating.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA94LA211