N5272A

Substantial
None

PIPER PA-23-160 S/N: 23-2109

Accident Details

Date
Friday, September 30, 1994
NTSB Number
CHI94LA351
Location
WEST CHICAGO, IL
Event ID
20001206X02232
Coordinates
41.880592, -88.219848
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

the pilot's failure to use the manual hydraulic pump to lower the landing gear. Factors were the failure of the fuel selector handle, the subsequent fuel starvation, and the pilot's failure to properly crossfeed and restart the left engine.

Aircraft Information

Registration
Make
PIPER
Serial Number
23-2109
Engine Type
Reciprocating
Year Built
1961
Model / ICAO
PA-23-160 PA23
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
5
FAA Model
PA-23-160

Registered Owner (Current)

Name
WELCH KEVIN R
Address
1018 PARKVIEW ST
City
HARTLAND
State / Zip Code
WI 53029-9332
Country
United States

Analysis

On September 29, 1994, about 2050 central daylight time, a Piper PA-23-160, N5272A, operated by Superstition Air Service of Mesa, Arizona, sustained substantial damage while landing at the DuPage Airport, West Chicago, Illinois. The commercial pilot and two passengers reported no injuries. The personal flight originated at 1845 in St Louis, Missouri, and was conducted under 14 CFR Part 91. A VFR flight plan was filed and visual meteorological conditions prevailed.

In his written statement, the pilot reported that he moved the left fuel selector from the auxiliary position to the main position during the descent. A few minutes later, the left engine began surging, then lost power. He unsuccessfully attempted to restore the engine power with the boost pump and crossfeed. The engine surged when the primer was pumped. He shut down the left engine and feathered the left propeller.

He reported that during the single engine approach, he lowered the landing gear handle and verified safe gear indications. During a "smooth and normal" landing, the nose gear collapsed at a speed of about 65 miles per hour. The airplane slid to a stop sustaining substantial damage to the lower nose structure.

During a telephone interview, the pilot reported that he did not pump the emergency hydraulic hand pump or activate the emergency extension system.

Examination of the airplane revealed that both main fuel tanks were about half full and the auxiliary tanks were nearly empty. Both electric fuel pumps, the crossfeed valve, and the right fuel selector operated normally. The rivets which mount the left fuel selector handle to the floor panel were pulled through the mount which allowed the handle to move freely without actuating the cable or fuel selector valve.

A landing gear retraction and extension test revealed no evidence of malfunction of the landing gear or hydraulic systems.

The pilot operating handbook for the PA-23-160 specifies in the emergency landing gear extension section "if the engine driven hydraulic pump fails, or the left engine driving the pump, extension of the landing gear or flaps is accomplished by supplying hydraulic pressure with the manual hydraulic pump. With gear or flap control in the desired position, 30-40 strokes of the pump handle will raise or lower the landing gear."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI94LA351