N6635C

Substantial
None

BEECH F33A S/N: CE-1028

Accident Details

Date
Tuesday, January 31, 1995
NTSB Number
LAX95LA090
Location
TUCSON, AZ
Event ID
20001207X02889
Coordinates
32.149715, -110.930274
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the student pilot's poor short field takeoff procedure and excessive nose rotation resulted in an inadvertent stall. A factor is the student pilot's lack of total experience.

Aircraft Information

Registration
N6635C
Make
BEECH
Serial Number
CE-1028
Engine Type
Reciprocating
Model / ICAO
F33A BE33
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
AIR TRANSPORT TRAINING INTL INC
Address
PO BOX 11420
Status
Deregistered
City
TUCSON
State / Zip Code
AZ 85734
Country
United States

Analysis

On January 31, 1995, at 1510 hours mountain standard time, a Beech F33A, N6635C, lost control and crashed shortly after lifting off runway 6L at Ryan Field, Tucson, Arizona. The pilot was conducting a local visual flight rules solo instructional flight. The airplane, registered to and operated by Air Transport Training International, Inc., Tucson, Arizona, sustained substantial damage. The student pilot was not injured. Visual meteorological conditions prevailed. The flight originated at Ryan Field at 1320 hours.

The operator told National Transportation Safety Board investigators in a telephone interview conducted on February 2, 1995, that the student pilot had flown to the practice area before returning to Ryan Field. The pilot returned to the airport and executed five full-stop landings and takeoffs.

On the last takeoff, the student pilot was executing a short field departure. The operator said the student pilot "overrotated" and the airplane stalled shortly after becoming airborne. The airplane initially struck the ground in a nose- and left wing-down attitude.

The pilot said in the aircraft accident report that he initially flew to the practice area. After practicing some maneuvers, he returned to Ryan Field and made three full-stop landings. On the fourth takeoff, he executed a short field takeoff. Shortly after raising the airplane nose, the stall warning horn sounded; one second later, the airplane struck the ground. The pilot reported no mechanical malfunctions.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX95LA090