N757JQ

Destroyed
Serious

CESSNA 152 S/N: 15279780

Accident Details

Date
Sunday, March 26, 1995
NTSB Number
BFO95LA036
Location
OAKLAND, MD
Event ID
20001207X03084
Coordinates
39.409183, -79.409744
Aircraft Damage
Destroyed
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the student pilot's abrupt remedial action during the aborted landing attempt. Related factors are the student pilot's lack of total experience, inadequate airspeed and the low altitude.

Aircraft Information

Registration
N757JQ
Make
CESSNA
Serial Number
15279780
Engine Type
Reciprocating
Model / ICAO
152 C152
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
PLANE AVIATION
Address
PO BOX 305
Status
Deregistered
City
MCHENRY
State / Zip Code
MD 21541
Country
United States

Analysis

On Sunday, March 26, 1995, at 1015 eastern standard time, a Cessna 152, N757JQ, operated as a solo instructional flight, collided with a tree during an aborted landing attempt at Garrett County Airport, near Oakland, Maryland. The student pilot, the sole occupant, was seriously injured and the airplane was destroyed. Visual meteorological conditions prevailed and no flight plan was filed. The flight was being operated under 14 CFR Part 91, and originated from Oakland, Maryland, exact time unknown.

The student pilot had completed several landings with the certificated flight instructor (CFI), and the CFI decided to approve the student pilot for solo flight. The student pilot completed three solo touch and go landings and was landing to a full stop when the accident occurred. According to a Federal Aviation Administration (FAA) Inspector, the CFI witnessed the accident. He reported that the airplane landed hard, then bounced and seemed to "float". The CFI stated that after full power was applied the airplane pitched down and impacted terrain left of the runway then nosed over.

The student pilot stated that at touchdown "...the front started to shimmy ... I tried giving more power and pulled back on the yoke. It did not help. I then decided to do a go around.... heard the stall buzzer going off. I looked down, saw my speed was down to 40, so I tipped my nose over to get my speed up..." The aircraft impacted the ground and came to rest inverted. Post accident examination of the aircraft by a FAA safety inspector revealed no anomalies. The student pilot reported 23 hours of total flight time.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO95LA036