N3298X

Substantial
None

CESSNA 310L S/N: 310L-0148

Accident Details

Date
Saturday, June 24, 1995
NTSB Number
CHI95LA199
Location
CRAWFORDSVILLE, IN
Event ID
20001207X03679
Coordinates
40.039714, -86.890129
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

the pilot's failure to maintain adequate airspeed during final approach to landing. A factor in the accident was the pilot's delayed action of aborting the landing.

Aircraft Information

Registration
N3298X
Make
CESSNA
Serial Number
310L-0148
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
310L C310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
TOUCH-N-GO FLYING CLUB INC
Address
4264 S 430 E
Status
Deregistered
City
KINGMAN
State / Zip Code
IN 47952-8037
Country
United States

Analysis

On June 24, 1995, at 1940 eastern daylight time, a Cessna 310L, N3298X, registered to the Engineering & Design Services, Inc., of West Layfayette, Indiana, was substantially damaged while landing at Crawfordsville Municipal Airport, Crawfordsville, Indiana. The pilot and two passengers reported no injuries. The airplane was being operated as a personal flight under 14 CFR Part 91 when the accident occurred. Visual meteorological conditions prevailed at the time and no flight plan was filed.

The pilot reported the flight was to be a proficiency flight. His intention was to stay in the airport traffic pattern and practice three takeoffs and landings. For his first landing, the pilot stated he decided to practice a power off landing. While on the downwind leg of the traffic pattern, he pulled both throttles to the idle position. "First landing was firm but decent, only I had to bring power in momentary on the base to make the runway," the pilot stated. The second pattern, he stated, was done without any addition of power, but he had to "...close in on the runway in order to make the runway... ." While on final to land, the pilot stated that he had to realign the airplane with the runway. He stated that at this point the airspeed dropped quickly, and he realized a "bad" situation. The pilot decided to perform a go around. "Abort was to late and I contacted the ground and dragged the left wing - abort was continued due to ground traffic directly ahead," the pilot stated. The third pattern was done using normal procedures and he landed the airplane with no further incidents.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI95LA199