Summary
On June 18, 1995, a Beech C24R (N24024) was involved in an incident near Houston, MS. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: PARTIAL LOSS OF ENGINE POWER DUE TO A FUEL INJECTOR BEING CLOGGED WITH CARBON. THIS RESULTED IN A LANDING ON UNSUITABLE TERRAIN.
On June 17, 1995, about 1945 central daylight time, a Beech C24R, N24024, registered to Jack W. Lewis, made a forced landing following partial loss of engine power shortly after takeoff from Houston Municipal Airport, Houston, Mississippi, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft received substantial damage and the private-rated pilot and one passenger were not injured. The flight was originating at the time of the accident.
The pilot stated that shortly after takeoff the engine began to sputter and lose power. He observed a field ahead and made a forced landing in the field. After rolling about 20 yards after touchdown the right main landing gear separated.
This incident is documented in NTSB report MIA95LA151. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N24024.
Accident Details
Probable Cause and Findings
PARTIAL LOSS OF ENGINE POWER DUE TO A FUEL INJECTOR BEING CLOGGED WITH CARBON. THIS RESULTED IN A LANDING ON UNSUITABLE TERRAIN.
Aircraft Information
Registered Owner (Historical)
Analysis
On June 17, 1995, about 1945 central daylight time, a Beech C24R, N24024, registered to Jack W. Lewis, made a forced landing following partial loss of engine power shortly after takeoff from Houston Municipal Airport, Houston, Mississippi, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft received substantial damage and the private-rated pilot and one passenger were not injured. The flight was originating at the time of the accident.
The pilot stated that shortly after takeoff the engine began to sputter and lose power. He observed a field ahead and made a forced landing in the field. After rolling about 20 yards after touchdown the right main landing gear separated. The nose gear separated and the left main gear collapsed. The aircraft then came to rest.
After the accident the engine was removed from the aircraft and placed on an engine test stand. The engine was started and would only operate to 1600 rpm. The fuel injectors were removed and the no. 6 fuel injector was found to be plugged with carbon. After cleaning all fuel injectors the engine was started and operated normally to full power.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA95LA151