N9775N

Substantial
None

BOTTERON Q-2 S/N: 2366

Accident Details

Date
Friday, July 14, 1995
NTSB Number
SEA95LA152
Location
ARLINGTON, WA
Event ID
20001207X04096
Coordinates
48.179431, -121.670242
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

THE NONPILOT-RATED MECHANIC'S IMPAIRMENT OF JUDGMENT AND PERFORMANCE DUE TO ALCOHOL; IMPROPER DECISION BY THE MECHANIC (UNQUALIFIED PERSON) TO FLIGHT CHECK THE AIRPLANE; AND FUEL EXHAUSTION AFTER TAKEOFF, DUE TO AN INADEQUATE SUPPLY OF FUEL.

Aircraft Information

Registration
N9775N
Make
BOTTERON
Serial Number
2366
Engine Type
None
Model / ICAO
Q-2 FK12
No. of Engines
0

Analysis

On July 13, 1995, at 1930 Pacific daylight time, an experimental Terry L. Botteron, Q-2, N9775N, experienced a loss of engine power shortly after takeoff from the Arlington Airport, Arlington, Washington. During the forced landing, the airplane landed hard on the runway. Visual meteorological conditions prevailed at the time and no flight plan was filed. The airplane was substantially damaged and the non-certificated pilot was not injured.

During an interview with the local police department and a Federal Aviation Administration Inspector from the Renton, Washington Flight Standards District Office, the pilot reported that he did not have a pilot's certificate and stated that the purpose of the flight was to test the airplane after performing maintenance.

Witnesses reported that shortly after the airplane took off, the engine began to sputter. The airplane made a right turn in the pattern and then made a low pass over the runway. The engine then quit, caught for a short time, then quit again. The pilot landed the airplane on a closed runway. During the landing, the airplane landed hard, collapsed the gear and skidded 81 yards before coming to a stop.

The police department performed a breathalyzer test which indicated .16 B.A.C.

A Federal Aviation Administration Inspector and two local mechanics inspected the airplane after the accident. The Inspector reported that the fuel tanks had been ruptured, however, there was no evidence of a fuel spill. The fuel lines and fuel filter were inspected and only a small amount of fuel was present. No evidence was found to indicate a mechanical failure or malfunction.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA95LA152